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Case History: First Isochronal Reservoir Test Successfully Performed Worldwide at a Bottomhole Temperature Greater than 430°F

机译:案例历史:首先在井底温度大于430°F的全球成功进行了第一等传储层测试

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Gujarat State Petroleum Corporation, Ltd (GSPC) recently decided to evaluate a reservoir in an offshore well on the Indian East Coast where the bottomhole temperature was higher than 433℉. The initial DST had shown significant potential for the zone of interest, and, therefore, GSPC decided to perform isochronal testing to obtain more detailed reservoir pressure information. In this environment, the DST tools would be required to function continuously in the high-temperature conditions for more than 16 days to retrieve the required data without interruption. These conditions would definitely challenge the capabilities of the currently available drill-stem testing (DST) equipment. This paper describes how DST tools rated to 450°F-bottomhole temperature and 15,000-psi differential pressure were configured to maintain integrity and successfully evaluate the well. The tools were annulus pressure responsive (APR) and would be operated with pressure applied to the annulus from the surface. The string included a multi-cycle downhole tester valve, a multi-cycle circulating valve, a blowout preventer (BOP) safety valve, a tubing tester valve, a secondary circulating valve, and safety circulating valves. The multi-cycle circulating valve added the flexibility of displacing the string with nitrogen for well stimulation if the well did not flow. The data describes the careful preparation of the tool string, the extreme conditions in which the DST tools had to operate to evaluate the well successfully, and how the meticulously-prepared tool string was capable of meeting GSPC's requirements. The DST tools performed satisfactorily for more than 16 days during the test. This job set a world record for the service company for a reservoir test performed in these high-temperature conditions and may have set a world record for all testing operations performed by other service companies as well. Advantages included elimination of coiled tubing, increased safety for this type of operation, and a reduction of rig time compared to other testing jobs.
机译:Gujarat State Petroleum Corporation,Ltd(GSPC)最近决定在印度东海岸的海上井中评估水库,其中井底温度高于433‰。初始DST表明显著潜在感兴趣的区域,因此,GSPC决定执行等时的测试,以获得更详细的储层压力的信息。在这种环境中,DST工具将需要在高温条件下连续运行超过16天以在不中断的情况下检索所需的数据。这些条件肯定会挑战目前可用的钻杆测试(DST)设备的能力。本文介绍了DST工具额定到450°F-井底温度和15,000psi差压的速度如何配置为维持完整性并成功评估井。该工具是环形压力响应(APR),并将在从表面施加到环空的压力下操作。该弦包括多周期井下测试阀,多周循环阀,井喷防喷器(BOP)安全阀,管道测试阀,次级循环阀和安全循环阀。如果井不流动,多周期循环阀增加了用氮气刺激氮气的柔韧性。这些数据描述了刀具串的仔细准备,DST工具必须运行的极端条件来评估成功良好的良好条件,以及精心准备的工具串如何满足GSPC的要求。 DST工具在测试期间超过16天令人满意地进行。这项工作为在这些高温条件下进行的储层测试的服务公司设置了世界纪录,并可能为其他服务公司执行的所有测试操作设定了世界纪录。优点包括消除线圈管,增加了这种类型的操作安全性,与其他测试作业相比减少了钻机时间。

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