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The Kvitebjorn Pipeline Repair

机译:kvitebjorn管道修复

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On the 1 of November 2007 during a routine inspection, severe anchor damage was discovered on the 30" Kvitebjorn rich gas pipeline, about 10 km from the platform at 210 m water depth. The damage constituted a localised dent and a 17deg buckle, but no leakage. Since 1987 Statoil on behalf of the different pipeline transportation licences, has invested time and money into building up an effective repair contingency for the pipeline network from the Norwegian Continental shelf, in particular the large gas export pipelines. The contingency repair method for the Kvitebjarn pipeline is based upon the use of two Morgrip couplings and a spool to be installed with remotely operated H-frames and a purpose build Coupling Installation Frame (CIF), constituting vital parts of the total Pipeline Repair System. The couplings were produced and tested back in 2005. This paper will cover the initial damage description, the repair preparations, the actual remote repair methodology and lessons learned. The Kvitebjern incident has shown how important it is to be prepared and it can be termed as a real baptism for the company's pipeline repair preparedness. The 27th of January 2009, one year and three months after the damage discovery, the repair was successfully completed and gas export from the Visund and Kvitebjern platforms resumed.
机译:在2007年11月1日在常规检查期间,在30“Kvitebjorn富有的汽油管道上发现了严重的锚损伤,距离平台约10公里,在水深210米。损坏构成了一个局部凹痕和17deg扣,但没有泄漏。自1987年以来代表不同的管道运输许可证,已投入时间和金钱从挪威大陆架,特别是大型天然气出口管道的管道网络的有效修复应急。的应急修复方法KVITEBJARN管道基于使用两个MORGRIP联轴器和阀芯,该阀芯安装有远程操作的H框架,并用途构建耦合安装框架(CIF),构成总管道修复系统的重要部分。生产和测试的联轴器回到2005年。本文将涵盖初始损害描述,修复准备,实际远程修复方法和经验教训。Th E KVITEBJERN事件表明了要准备的重要性,它可以被称为公司管道修复准备的真正洗礼。 2009年1月27日,一年和三个月损坏发现后,修复成功完成,恢复了「昆榜和KviteBjern平台的天然气出口。

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