首页> 外文会议>ASME international conference on ocean, offshore and arctic engineering >ANALYSIS OF WELLBORE INSTABILITY IN AN OFFSHORE FIELD: A CASE STUDY
【24h】

ANALYSIS OF WELLBORE INSTABILITY IN AN OFFSHORE FIELD: A CASE STUDY

机译:海上油田井壁失稳分析:案例研究

获取原文

摘要

Several wellbore instability problems have been encountered during drilling a shale formation in an offshore field, leading to the collapse of the main borehole and resulting in several sidetracks. In this study, an integrated 1D & 3D Geomechanical model was built for the field in order to investigate the major factors that control the instability problems from a Geomechanical point of view and to design an optimum mud window for planned wells in the field. Effect of bedding on wellbore stability was the most important factor to explain the observed drilling events. Optimized well paths for planned wells were proposed based on results of a sensitivity analysis of the effect of bedding orientation on wellbore stability. It has been observed that bedding exposed depends not only on well inclination but also on dip of the formation, attack angle, and azimuth.
机译:在海上油田页岩地层钻井过程中遇到了几个井眼失稳问题,导致主井眼坍塌,并导致了一些侧向钻进。在这项研究中,为现场建立了一个集成的1D和3D地质力学模型,以便从地质力学的角度研究控制失稳问题的主要因素,并为现场计划中的油井设计最佳的泥浆窗口。地层对井筒稳定性的影响是解释观察到的钻井事件的最重要因素。根据层理取向对井眼稳定性影响的敏感性分析结果,提出了计划井的优化井径。已经观察到,裸露的地层不仅取决于井的倾斜度,还取决于地层的倾角,攻角和方位角。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号