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Improving Reliability and Boosting Energy Efficiency of an Ammonia Plant by Revamping Natural Gas Pipe Line and Associated Compressor Train

机译:通过改建天然气管道和相关压缩机组来提高氨厂的可靠性并提高能效

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Petrokemija's ammonia plant has been in operation since 1983 and designed to use low pressure natural gas of 7 barg (101.5 psig) at the inlet of natural gas compressor train. The new possibility to extract higher pressure natural gas of 30 barg (435.1 psig) from natural gas pipeline network triggered revamping scenario to boost the energy efficiency and improve reliability. In total, the overall natural gas consumption of ammonia plant was reduced for 1200 Sm?/h which gives 2.1 % better energy efficiency at nameplate production rate. The revamping process from concept to commissioning is presented, including planning, procurement, installation, commissioning, safety procedures and practical difficulties which encountered during startup. Although safety comes first as a part of each and every revamping process phase including developing a risk analysis matrix and HAZOP study, our experience shows that occurred leakage of natural gas during startup could jeopardize the complete plant safety, and even further steps should be taken in order to eliminate all possible risks.
机译:Petrokemija的氨厂自1983年开始运营,其设计目的是在天然气压缩机列的进口处使用7 barg(101.5 psig)的低压天然气。从天然气管道网络中提取30 barg(435.1 psig)高压天然气的新可能性引发了改造方案,以提高能源效率并提高可靠性。总的来说,氨厂的天然气总消耗量减少了1200 Sm2 / h,在铭牌生产速度下,能源效率提高了2.1%。介绍了从概念到调试的整个改造过程,包括计划,采购,安装,调试,安全程序以及启动过程中遇到的实际困难。尽管安全是每个改造过程阶段的一部分,包括制定风险分析矩阵和HAZOP研究,但我们的经验表明,启动过程中发生的天然气泄漏可能会危害整个工厂的安全,甚至应采取进一步措施。为了消除所有可能的风险。

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