首页> 外文会议>Congress on forensic engineering >ANALYSIS OF SUBSIDENCE AND RESULTING DAMAGE OVER AN AREA FOR 3 DECADES
【24h】

ANALYSIS OF SUBSIDENCE AND RESULTING DAMAGE OVER AN AREA FOR 3 DECADES

机译:分析沉降和导致面积损坏3年

获取原文

摘要

This paper presents an investigation conducted into the cause of collapse and the resulting subsidence and associated damage. The project is located in the East St. Louis area of Illinois. The study consisted of 3 subsurface investigations conducted into the old works over about a 30 year time period and numerous surface investigations. The old works are in the No. 6 Coal Seam in the Illinois Coal Basin which is about 2 m thick, and were mined between the years 1900 to 1925. The depth of the old works is about 60m deep. At the project site there is up to about 50 m of soil overburden.Over the course of the 3 decade investigation period, extensive flooding of the abandoned workings was observed resulting in mine floor softening. Considering the softened floor condition, a bearing capacity of less than one was calculated and appears to be clearly the mode of failure. The paper discusses the floor stratigraphy and rock mechanics properties used in the analysis. The paper also discusses the resulting subsidence events and associated damage. As a result of the damage from one of the subsidence events, a state police headquarters building had to be razed. Also, the measured ground movements of the most recent subsidence are correlated with the rate of damage experienced by the recreational building. This structure exists in the tension zone of the sag subsidence and has consequently been subjected to hogging and tension related damage. The thick soil cover has significantly contributed to the draw zone width which has affected this building. In investigating the subsidence movements and the damage in this building, the measured ground displacements were quantified by angular distortion and compared to the damage over time.
机译:本文介绍了对崩溃原因进行的调查以及所产生的沉降和相关损害。该项目位于伊利诺伊州的东路圣路易斯地区。该研究包括在旧作品中进行的3个地下调查,超过约30年的时间段和许多表面调查。旧作品位于伊利诺伊州煤盆中的6号煤层,大约2米厚,在1900年至1925年之间开采。旧作品的深度约为60米。在项目现场,土壤覆盖率高达约50米的土壤覆盖物。在3年的十年调查期间,观察到遗弃废弃的工作的广泛洪水导致矿井疲软。考虑到软化的地板条件,计算均承载能量小于一个,似乎显然是故障模式。本文讨论了分析中使用的地板地层和岩石力学性质。本文还讨论了所产生的沉降事件和相关损害。由于其中一个沉降事件造成的损害,州警察总部大楼必须夷为平地。此外,最近沉降的测量地面运动与休闲建筑所经历的损害率相关。这种结构存在于凹陷沉降的张力区,因此受到摇动和紧张相关的损伤。厚的土壤覆盖率显着促进了影响这座建筑物的拉伸区宽度。在调查沉降运动和该建筑物中的损坏时,测量的地位移通过角度变形来量化,与损伤随时间造成相比。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号