首页> 外文会议>Corrosion conference and expo;Corrosion 2012 >Beneficial Effects of Chemical Treatment and Maintenance Pigging Programs in Returning an Offshore Pipeline to Pre-Hurricane Ike Conditions Following a Breach and the Ingress of Seawater and Sand, and the Effects of Bacteria Generated H_2S
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Beneficial Effects of Chemical Treatment and Maintenance Pigging Programs in Returning an Offshore Pipeline to Pre-Hurricane Ike Conditions Following a Breach and the Ingress of Seawater and Sand, and the Effects of Bacteria Generated H_2S

机译:化学处理和维护清管程序在破坏和海水和沙子进入后使海上管道恢复到飓风之前的状况的有益效果,以及细菌产生的H_2S的影响

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When Hurricane Ike crossed the Gulf of Mexico in September 2008, one of the major laterals in an offshore gas gathering system was ripped from the trunkline. As a consequence of that breach, approximately 75,000 BBL (11.9 MM liters) of seawater entered the trunkline, and approximately 40,000 BBL (6.4 MM liters) of seawater entered the lateral. A previous paper (NACE #10064) described the repairs, the high levels of hydrogen sulfide (H_2S) that were generated by microbiological activity, the monitoring program, and the chemical treatment and maintenance pigging programs, which were implemented to re-establish control over the SRBs and the H_2S they generated. This paper is a follow up to that report. Although inhibitor residuals have been very high, sand production appears to have temporarily increased as the sand from within the lateral and trunkline is slowly transported uphill to the onshore gas processing facility, "one girth weld at a time." Of interest, the iron counts have become elevated. This may be attributed to the maintenance (cleaning) pigs, which are slowly pushing the sand that entered the pipelines when the pipeline was breached. The pigs, coupled with the transportation of the sand, are apparently scraping and "sand blasting" the walls of the trunkline, thus removing the oxides and corrosion products from the pipeline. This paper also presents results from destructive metallurgical examination of a hot tap coupon or "cut-out" obtained from the trunkline when a new 6" (15.2 cm) OD subsea tie-in (SSTI) was made at the 3:00 o'clock orientation in 2010.
机译:当艾克飓风于2008年9月越过墨西哥湾时,海上天然气收集系统的主要分支之一从干线上被扯掉了。由于该破坏,大约75,000 BBL(11.9 MM升)的海水进入了干线,大约40,000 BBL(6.4 MM升)的海水进入了支管。先前的论文(NACE#10064)描述了维修,微生物活动产生的高浓度硫化氢(H_2S),监控程序以及化学处理和维护清管程序,这些程序的实施是为了重新建立对它们生成的SRB和H_2S。本文是该报告的后续报告。尽管抑制剂的残留量非常高,但是随着侧向和主干内的砂子缓慢地上坡运输到陆上天然气处理设施,“一次一次环焊”,砂子的产量似乎暂时增加了。有趣的是,铁的数量已经增加。这可能归因于维护(清洁)清管器,当管道破裂时,它们会缓慢推动进入管道的沙子。显然,清管器与沙子的运输一起正在刮擦和“喷砂”干线的壁,从而从管道中清除了氧化物和腐蚀产物。本文还介绍了在3:00 o'制作了新的6英寸(15.2厘米)外径的海底接头(SSTI)时,对从干线获得的热抽头或“切口”进行的破坏性冶金学检查结果。 2010年的时钟定位。

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