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MINIPILES AND JET-GROUTING: A STRONG FOUNDATION IN PARMA, ITALY

机译:迷你派和射箭灌浆:意大利帕尔马市的坚实基础

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The objective of the € 200 million ($280 million) project Parma Railways Station-Urban Transformation was the reconnection of the North and South parts of the town by constructing an 80 m (250 ft) wide sunken artery passing under the four double railway tracks of the station without any impact on train traffic. The site of the project, adjacent to the Parma River, presented water seepage problems at any excavation depth. The use of conventional large diameter bored pile machinery was not allowed by the Railway Authority because equipment dimension and construction phases do not comply with train traffic safety regulations. Foundations for the bypass were thus constructed by minipiles nested into jet-grouted soil using machinery operating within the existing head room and at a safe distance from the tracks. Jet-grouting treatment reached depths of 25 to 28 m (80 to 90 ft) from tracks' grade and embedded minipile heads were terminated at 2 to 3 m (6.6 to 10 ft) below grade. Load tests on minipiles were pushed to failure. Failure occurred at a 240 t (265 t) load without breakage of the bond between the jet grouted soil and the minipiles. A 0.93 MPa (135 psi) shear resistance "t" between minipile steel casing and the jet-grouted soil was measured prior to the failure of the steel casings. Overall measured foundation settlements were well within expected values and were considered insignificant.
机译:耗资2亿欧元(2.8亿美元)的帕尔马铁路站-城市改造项目的目标是,通过在一条两条铁路的四条双线轨道下修建一条80 m(250 ft)宽的下沉动脉,重新连接该镇的北部和南部。该车站对火车交通没有任何影响。该项目的地点毗邻帕尔马河,在任何开挖深度都存在渗水问题。铁道当局不允许使用常规的大直径钻孔桩机械,因为设备尺寸和施工阶段不符合火车交通安全法规。因此,通过使用在现有净空室内操作并与轨道保持安全距离的机械,将微型桩嵌套在喷射注浆的土壤中,从而为旁路建造基础。喷射注浆处理距轨道的坡度深度为25至28 m(80至90英尺),嵌入式微型桩头在坡度以下2至3 m(6.6至10英尺)处终止。微型桩上的负载测试已失败。在240吨(265吨)的载荷下发生了破坏,而喷射灌浆的土壤与微型桩之间的粘结没有破裂。在钢制外壳失效之前,测量了微型钢制外壳与喷射灌浆土壤之间的抗剪强度“ t”为0.93 MPa(135 psi)。整体测得的地基沉降均在预期值范围内,被认为是微不足道的。

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