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Investigation of Fully Grouted Roof Bofts Installed Under In Situ Conditions

机译:在现场条件下安装全灌浆顶棚锚杆的研究

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The National Institute for Occupational Safety ane Health (NIOSH) Pittsburgh Research Laboratory (PRL) is continuing to investigate the behavior of fully grouted roof bolts in the weak roof rock of the Safety Research Coal Mine (SRCM). This paper describes the results of three studies: 1. A series of 24 pull tests of bolts installed fully grouted and overcored to leave 12 inches of grouted bolt. The tests compared the pull-out performance of offset-head roof bolts with that of standard 5/8-inch bolts; 2. A second series of 24 tests that compared the pull-out loads obtained by bolts installed with 1 ft of resin (a Short Encapsulation Pull Test or SEPT) to that of fully grouted bolts overcored to leave only 12 inches of grouted bolt, and; 3. An investigation into the pressures generated during the installation of fully grouted resin bolts All of the bolts installed and pulled were overcored and removed from the roof after the pull tests to allow inspection of the resin. The first study found that there was no significant difference in pullout load between the offset-head bolts and the standard bolts. The second study, comparing the SEPT bolts and the partially-overcored fully grouted bolts, indicated that SEPT can significantly underestimate bolt anchorage grip factor, suggesting that the SEPT is a conservative measure of actual bolt performance. Significant loss of resin to cracks in the roof was observed in the bolts overcored in the SRCM. The third study explored one possible explanation for the resin loss, high pressures generated during bolt installation. These tests employed bolts installed in strain gauged steel tubes. The results confirmed that significant pressures (greater than 4,000 psi) can be generated during bolt installation. The results of the pressure tests, combined with the observations of resin loss in bolts installed in the SRCM, suggest that under some circumstances resin loss and under-encapsulation could take place and lead to degraded bolt performance. Glove fingering was observed in all recovered bolts to various degrees. The limited comparative data suggested that the effect of glove fingering ranged from slight to moderate. Complete mixing of the resin was observed on all of the 40 bolts recovered (28 fully grouted and 12 SEPT) Australian and U.S resins were compared and the Australian resins were observed to have much smaller catalyst compartment areas and lower resin viscosities. These differences are suggested as potential explanations for occasional resin mixing problems noted in Australian resin bolt installations
机译:美国国家职业安全与健康研究所(NIOSH)匹兹堡研究实验室(PRL)仍在继续研究安全研究煤矿(SRCM)的弱顶岩中完全注浆的顶板锚杆的性能。本文介绍了三项研究的结果:1.一系列的24个完全灌浆并过芯的螺栓拉力测试,留出12英寸的灌浆螺栓。测试比较了偏头屋顶螺栓和标准5/8英寸螺栓的拉出性能。 2.第二组共24个测试,比较了安装有1英尺树脂的螺栓所产生的拉力载荷(短封装拉力测试或SEPT)与完全注浆的螺栓芯(仅留有12英寸的注浆螺栓)的拉拔载荷,以及; 3.调查完全灌浆的树脂螺栓在安装过程中产生的压力。在进行拉力试验后,所有安装和拉动的螺栓都被过度套芯并从屋顶取下,以便检查树脂。首次研究发现,偏头螺栓和标准螺栓之间的拔出载荷没有显着差异。第二项研究比较了SEPT螺栓和部分压实的全灌浆螺栓,结果表明SEPT可以大大低估螺栓的锚固抓地力因子,这表明SEPT是实际螺栓性能的保守指标。在SRCM中超芯的螺栓中,树脂明显损失到了屋顶的裂缝。第三项研究探讨了树脂损失,螺栓安装过程中产生的高压的一种可能解释。这些测试使用安装在应变计钢管中的螺栓。结果证实,在螺栓安装过程中会产生很大的压力(大于4,000 psi)。压力测试的结果,加上对SRCM中安装的螺栓中树脂损失的观察,表明在某些情况下可能发生树脂损失和封装不足,并导致螺栓性能下降。在所有回收的螺栓中均以不同程度观察到手套指法。有限的比较数据表明,手套指法的影响范围从轻微到中等。在回收的所有40个螺栓(28个完全灌浆和12个SEPT)上观察到树脂完全混合,比较了澳大利亚和美国的树脂,并观察到澳大利亚的树脂具有较小的催化剂隔室面积和较低的树脂粘度。这些差异被建议作为澳大利亚树脂螺栓装置中偶尔出现的树脂混合问题的潜在解释。

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