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Elimination of Biogenic Hydrogen Sulfide in Underground Gas Storage. A Case Study

机译:消除地下储气库中的生物硫化氢。案例研究

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The paper reports microbiological study of Sulfate Reducing Bacteria activity in underground gas storage and preventive action against H_2S formation. Complex research was performed on natural gas reservoir in Swarzow, where one of a few gas storages in Poland had been arranged. The presence of hydrogen sulfide in the 10-th cycle of UGS exploitation gave impact to search a new effective methods which might limit the microbial processes of sulfate reduction in the reservoir. Having the long-term experience, in 1995-96 operation of biocide treatment in SWARZOW UGS was completed with success. Selective biocides (quaternary ammonium compounds) were applied into the reservoir for the first time in Poland, in accordance with patented technology worked out in Oil and Gas Institute, Department of Microbiology. In 1997-98 the biocide injections to exploitation wells were repeated. These operations conduced to the total elimination of Sulfate Reducing Bacteria from the formation waters and caused partial reduction of H_2S content in natural gas recovered from the reservoir. In 2003 the new technology based on synergetic action of biocide, represented by triazine derivatives, and H_2S Scavenger (Sulfa Clear) was implemented for the first time in underground environment. Practical application of this technology on 2 objects of UGS was finished with a great success. Content of hydrogen sulfide in the recovered gas and formation waters now accords with European Standards. The paper also discusses microbiological studies of processes observed in the natural gas reservoir in Wierzchowice, which is the largest store in Poland. Its final capacity will be ca. 4,3 billion cubic meters of natural gas. The research was conducted between the 1st and the 8th cycle of UGS exploitation. Present investigations were performed in the monitoring system and included microbiological and chemical analysis of formation waters and drilling fluids. Active strains of H_2S producing bacteria (Desulfovibrio sp. And Desulfotomaculum sp.) isolated from the reservoir, have been used for testing biocides selected to protect exploitation wells of WIERZCHOWICE UGS.
机译:该论文报道了地下储气库中硫酸盐还原菌活性的微生物学研究以及对H_2S形成的预防作用。在Swarzow的天然气储层进行了复杂的研究,波兰的一些储气库已被安排在那里。在UGS开采的第10个循环中存在硫化氢,对寻找一种新的有效方法产生了影响,该方法可能会限制储层中硫酸盐还原的微生物过程。凭借长期的经验,SWARZOW UGS中的杀菌剂处理于1995-96年成功运行。根据微生物学石油与天然气研究所的专利技术,在波兰首次将选择性杀生物剂(季铵化合物)应用于该储层。在1997-98年,重复向杀伤井中注入杀生物剂。这些操作导致从地层水中完全消除硫酸盐还原细菌,并导致部分降低了从储层中回收的天然气中的H_2S含量。 2003年,首次在地下环境中实施了以三嗪衍生物为代表的基于杀生物剂协同作用的新技术和H_2S清除剂(Sulfa Clear)。该技术在UGS的两个对象上的实际应用取得了巨大成功。现在,回收气和地层水中的硫化氢含量符合欧洲标准。本文还讨论了在Wierzchowice天然气储层中观察到的过程的微生物学研究,Wierzchowice是波兰最大的储气库。其最终容量将为。 43亿立方米天然气。该研究是在UGS开发的第一个周期和第八个周期之间进行的。目前的调查是在监测系统中进行的,包括地层水和钻井液的微生物学和化学分析。从储层中分离出的产生H_2S的活跃细菌(Desulfovibrio sp。和Desulfotomaculum sp。)已用于测试为保护WIERZCHOWICE UGS开采井而选择的杀菌剂。

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