首页> 外文会议>Turbomachinery symposium >PRACTICAL USE OF ROTORDYNAMIC ANALYSIS AND TROUBLESHOOTING SKILLS TO CORRECT A LONG-TERM SYNCHRONOUS VIBRATION PROBLEM IN AN OVERHUNG TURBOBLOWER
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PRACTICAL USE OF ROTORDYNAMIC ANALYSIS AND TROUBLESHOOTING SKILLS TO CORRECT A LONG-TERM SYNCHRONOUS VIBRATION PROBLEM IN AN OVERHUNG TURBOBLOWER

机译:转子动力学分析和故障排除技巧在纠正悬臂式涡轮机长期同步振动问题中的实际应用

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The two subject blowers operate in parallel to circulate wet chlorine gas. Both units had large synchronous vibrations that led to multiple bearing failures. After simple rotordynamics studies failed to identify the problem, a comprehensive model that accounted for both the motor and blower was successful at identifying the problem as high sensitivity to unbalance loads due to an extremely lightly-loaded (less than one pound) condition at the blower's inboard bearing (refer to Gutzwiller and Corbo, 2001). Based on the results of the rotordynamic analysis, two changes were made to both units. The couplings were changed from disk to gear couplings, and the blower's bearings were changed from plain cylindrical to tilting-pad designs. After implementing these changes, unit "A" ran smoothly for a period of six weeks, in accordance with the predictions of the rotordynamic analysis, and it appeared to all that the problem was completely solved. However, when the "B" blower was then started up the two machines then commenced a three month period of operation in which each suffered from intermittent periods of high synchronous vibrations. During this time, the following behavior traits, which can only be described as bizarre, were observed: 1. After a smooth startup, vibration increased to a high level after about one week. 2. The transition from low vibrations to high vibrations was almost instantaneous. Additionally, this transition was always accompanied by an axial motion of the blower rotor away from the active thrust bearing. 3. The units appeared to be more likely to suffer high vibrations when both were running simultaneously. 4. Starting one machine might result in increased vibrations on the other, and shutting down a machine might lower vibrations on the other. 5. Someone observed that during a rainstorm the vibration levels decreased. (Note: the blowers are located outside.) Spraying water on the bearings sometimes (but not always) had a similar effect. A task force of experts was then commissioned and an extensive troubleshooting effort commenced. Some of the potential root causes that were hypothesized included blower surging, starvation of the tilting-pad bearings, thermally-induced misalignment, insufficient blower thrust, acoustic resonance, axial vibration, seal rubbing, and Morton effects. After an extensive troubleshooting effort that included more rotordynamic analysis, bearing flow analysis, blower thrust analysis, and extensive studying of orbit plots, spectrum plots, and vibration and temperature histories, the task force concluded that the most likely cause was rubbing at the blower's carbon ring seal. Accordingly, the seal was disassembled and its locating pins were found to have come loose and generated a rub. Design changes were then implemented to provide better retention for the pins. The units were then restarted and it was verified that the modifications had finally eliminated the vibration problems. This paper shows how the combination of rotordynamic analysis and troubleshooting skills was employed to identify and generate corrective actions for two independent causes of high synchronous vibrations.
机译:两台鼓风机并联运行以循环湿氯气。两个单元均具有较大的同步振动,从而导致多个轴承故障。在简单的转子动力学研究未能识别出问题之后,考虑了电动机和鼓风机的综合模型成功地将问题识别为对鼓风机的极轻负载(小于1磅)状况造成的对不平衡负载的高度敏感性。内侧轴承(请参阅Gutzwiller和Corbo,2001年)。根据转子动力学分析的结果,两个单元都进行了两次更改。联轴器从盘式联轴器更改为齿轮联轴器,鼓风机的轴承从普通圆柱体更改为倾斜垫设计。完成这些更改后,根据转子动力学分析的预测,“ A”单元顺利运行了六周,并且看来问题已完全解决。但是,当启动“ B”鼓风机时,两台机器随后开始运行三个月,其中每一个都遭受间歇性的高同步振动。在这段时间内,观察到以下行为特征,这些行为特征只能描述为怪异的:1.平稳启动后,大约一周后振动增加到很高的水平。 2.从低振动到高振动的转变几乎是瞬时的。另外,这种过渡总是伴随着鼓风机转子离开主动止推轴承的轴向运动。 3.当两个单元同时运行时,它们似乎更有可能遭受高振动。 4.启动一台机器可能会导致另一台机器的振动增加,而关闭机器可能会降低另一台机器的振动。 5.有人观察到,在暴雨期间,振动水平降低了。 (注意:鼓风机位于室外。)有时(但并非总是)在轴承上喷水具有类似的效果。然后委托了一个专家小组,并开始了广泛的故障排除工作。推测的一些潜在根本原因包括鼓风机喘振,可倾瓦轴承饥饿,热引起的未对准,鼓风机推力不足,声共振,轴向振动,密封件摩擦和莫顿效应。经过广泛的故障排除工作,包括更多的转子动力学分析,轴承流量分析,鼓风机推力分析以及对轨道图,频谱图以及振动和温度历史的广泛研究,工作队得出结论认为,最可能的原因是鼓风机的碳摩擦密封圈。因此,拆卸了密封件,发现其定位销松动并产生了摩擦。然后进行设计更改,以提供更好的插针固定性。然后重新启动设备,并确认修改最终消除了振动问题。本文展示了如何结合使用转子动力学分析和故障排除技能来识别和生成针对高同步振动的两个独立原因的纠正措施。

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