【24h】

A STUDY ON A CLUSTERED LINEAR AEROSPIKE-NOZZLE COMBUSTOR

机译:聚类线性气雾喷嘴燃烧室的研究

获取原文

摘要

To clarify fundamental issues of linear aerospike nozzle engines, a ground level combustion test with a linear aerospike nozzle combustor composed of two 3-clustered-cell-nozzles and a truncated-spike-nozzle was conducted. The combustor has a nominal thrust of 14 kN, a maximum chamber pressure of 5.0 MPa, and utilizes LOX and methane as propellants. The obtained thrust coefficient efficiency,ηCF, at a ground condition was only about 87.5% in comparison with a prediction of 97.0%. To find the cause of this large performance loss, a cold flow test with a subscale model of the 3-clustered-cell-nozzles was conducted. A simple analysis with these results suggested that the losses due to gaps of cell nozzles and cell-to-cell interaction were one of the main causes of this performance loss.
机译:为了弄清线性气钉喷嘴发动机的基本问题,进行了一个由两个3簇式气室喷嘴和一个截短的尖钉喷嘴组成的线性气钉喷嘴燃烧室进行的地面燃烧试验。燃烧室的额定推力为14 kN,最大腔室压力为5.0 MPa,并利用LOX和甲烷作为推进剂。在地面条件下获得的推力系数效率ηCF仅约为87.5%,而预测值为97.0%。为了找出造成这种巨大性能损失的原因,我们进行了使用3簇细胞喷嘴的小规模模型进行的冷流测试。对这些结果的简单分析表明,由于电池喷嘴间隙和电池间相互作用而造成的损耗是造成这种性能下降的主要原因之一。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号