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BLAST FURNACE THERMAL CONTROL AND AERODYNAMIC MONITORING USING ADVANCED SIGNAL PROCESSING METHODS, IN CORUS UK

机译:使用英国先进的信号处理方法对高炉进行热控制和气动监测

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On line expert systems are employed in the control and monitoring of Redcar's 14m blast furnace and Scunthorpe's Queens Anne and Victoria, both of which are 9m blast furnaces. The expert systems at both plants are based on the standard G2 platform from Gensym. The objective of the installed systems is to both standardise and improve the quality of metallurgical process control decision-making. Most aspects of furnace operation are monitored including hearth liquid levels, raw materials quality, wall accretion monitoring and cooling water leakage. Trend analysis is applied to both top gas hydrogen and under-tuyere temperatures to determine whether cooling water leakage is entering the furnace. Thermal control and aerodynamic monitoring however form the central core of the systems and it is these aspects that are considered in this paper. Thermal control: Both plants adjust the injectant rate set point at regular intervals to compensate for variations between the achieved injectant rate and the set point. These variations are caused by changes in specific oxygen consumption due to direct reduction variability. At Redcar, changes are also made in response to significant drift in direct reduction by comparing the long and short-term trend. This has prevented significant reductions in hot metal quality. At Scunthorpe, a statistical process control approach is applied to enable or disable further changes to the injectant rate based on actual and predicted metal quality. The reduction in the frequency of changes, and more appropriate changes, has yielded a reduction in hot metal silicon variability of around 10%. Aerodynamic monitoring: Results from the recent 5th Framework CHEM project are described. Multivariate SPC models, generated using principal component analysis, are used to monitor process stability. Stack pressure differentials and top gas analysis signals are the key variables. A G2 module has been developed to run such models on line and undertake contribution analysis when warning or action limits are exceeded. The module allows identification of the signals that have changed most significantly. A second module has also been developed in G2 to classify the trend in each of the two principal components by generating a sequence of discrete events, which can then be analysed. Using both of these techniques it was possible to predict the most significant slips and channels over a 2-year period. Management and implementation issues are discussed, in particular the stepwise introduction of new procedures, and the style and content of the advice given. Clear simple action messages are required with supporting information displayed on supplementary workspaces.
机译:在线专家系统用于Redcar的14m高炉和Scunthorpe的Queens Anne和Victoria的控制和监视,这两个都是9m的高炉。两家工厂的专家系统均基于Gensym的标准G2平台。已安装系统的目标是标准化和提高冶金过程控制决策的质量。监测熔炉运行的大多数方面,包括炉底液位,原料质量,壁厚监测和冷却水泄漏。趋势分析适用于炉顶氢气和风口温度,以确定冷却水泄漏是否进入炉内。但是,热控制和空气动力学监控构成了系统的核心,本文正是考虑了这些方面。热控制:两家工厂均定期调整喷射速率设定点,以补偿所达到的喷射速率与设定点之间的差异。这些变化是由于直接还原变化引起的单位氧气消耗量的变化引起的。在雷德卡(Redcar),还通过比较长期趋势和短期趋势来对直接减少量的显着变化做出响应。这防止了铁水质量的显着降低。在斯肯索普(Scunthorpe),基于实际和预测的金属质量,采用了统计过程控制方法来启用或禁用对注入速率的进一步更改。变化频率的降低以及更适当的变化已使铁水硅变异性降低了约10%。空气动力学监测:描述了最近的第5框架CHEM项目的结果。使用主成分分析生成的多变量SPC模型用于监视过程稳定性。烟囱压力差和顶部气体分析信号是关键变量。已经开发了一个G2模块来在线运行此类模型,并在超出警告或操作限制时进行贡献分析。该模块允许识别变化最大的信号。在G2中还开发了第二个模块,通过生成一系列离散事件来对两个主要成分中的每个趋势进行分类,然后可以对其进行分析。使用这两种技术,可以预测两年内最重要的滑移和通道。讨论了管理和实施问题,尤其是逐步引入新程序以及所提供建议的样式和内容。需要清晰的简单操作消息,并在补充工作空间上显示支持信息。

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