首页> 外文会议>International Conference on Continuous Casting of Steel in Developing Countries(CCC'04); 20040914-17; Beijing(CN) >Recent Improvement of Continuous Casting Practice for High Quality Free Surface Defect Slab Product of Gas Cylinders Application
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Recent Improvement of Continuous Casting Practice for High Quality Free Surface Defect Slab Product of Gas Cylinders Application

机译:气瓶应用中高质量无表面缺陷板坯产品连铸实践的最新改进

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Due to high crack sensitivity of slab product of gas cylinders application, its continuous casting process and alloy composition were continuously evaluated and then improved to overcome its critical solidification process. The study was conducted at CC No.3 Slab Steel Plant Krakatau Steel. The purpose was to improve slab surface quality by reducing surface defects such as longitudinal, transverse and star crack so that the slab surface doesn't need to be totally scarfed. The method applied was by performing plant trial process, which the casting parameters such as casting powder selection, metallurgical cooling, mould level control, superheat and casting speed were continuously monitored and then adjusted to the surface quality of the product. The casting powder selected has lower viscosity and melting point than the previous one. The water quantity was reduced from 0.67 l/kg to 0.58. l/kg at casting speed of 1.1 m/minute. The mould level was controlled in the range of +- 5%. The casting speed was dynamically adjusted to the temperature condition. In addition the chemical composition such as carbon was designed to achieve optimum casting parameters by setting the carbon content less than 0.09% in order to avoid the peritectic grade. The results of the study are decreased surface defect quantity, free intercolumnar crack and smooth casting process. The quantity of the transverse and longitudinal crack decreased by almost 90%. The star crack was reduced from 62.21 % to 28.87 %. The slab surface scarfed was significantly reduced from 85.54 % to less than 25%. The yield loss per slab of the steel decreased from 3.4 % to 0.05 %. These new casting parameters and developed alloy composition are then used and standardized for the mass production of the steel.
机译:由于气瓶板坯产品对裂纹的敏感性高,因此对其连续铸造工艺和合金成分进行了连续评估,然后对其进行改进以克服其关键的凝固过程。该研究是在CC第三板坯钢铁厂Krakatau Steel进行的。目的是通过减少表面缺陷(例如纵向,横向和星状裂纹)来改善板坯表面质量,从而不必完全刮除板坯表面。所采用的方法是通过进行工厂试验过程来进行的,其中连续监测铸造参数,例如铸造粉末的选择,冶金冷却,结晶器液位控制,过热度和铸造速度,然后根据产品的表面质量进行调整。所选择的铸粉的粘度和熔点比前一种低。水量从0.67 l / kg减少到0.58。铸造速度为1.1 m / min时为l / kg。模具水平控制在±5%的范围内。铸造速度被动态地调节到温度条件。另外,通过将碳含量设定为小于0.09%,可以避免包晶层的出现,从而设计出化学成分(例如碳)以获得最佳的铸造参数。该研究的结果是减少了表面缺陷量,自由的柱间裂纹和光滑的铸造工艺。横向和纵向裂纹的数量减少了近90%。星状裂纹从62.21%减少到28.87%。板结表面的结疤率从85.54%显着降低到25%以下。每块钢的屈服损耗从3.4%降低到0.05%。然后将这些新的铸造参数和开发的合金成分用于钢的批量生产并进行标准化。

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