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Hydrate Formation in Chevron Mabee Unit for NGL Recovery and CO_2 Purification for EOR

机译:Chevron Mabee装置中的水合物形成,用于NGL回收和EOR的CO_2净化

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In the early 1990’s, Chevron installed a new process to recover natural gas liquids (NGLs) from recycledrnCO_2 in their Rangely Weber Sand Unit. The facility was designed based on a patent issued in June ofrn1988 (U.S. Patent # 4,753,666). The process, as claimed in the patent, used a refluxed distillation towerrnto produce an overhead stream virtually free of n-butane and heavier components and a bottomsrnstream containing the majority of the heavier components. Based on the success of the Rangley plant’srnoperation, a similar facility was designed and fabricated by Dickson Process Systems and installed inrnChevron’s Mabee field near Midland, Texas.rnWhen the Mabee plant faced some unique challenges in the NGL Recovery unit, Chevron contactedrnDickson Process Systems, Bryan Research & Engineering (BR&E), and Sulzer Chemtech USA to helprntroubleshoot the process to operate as designed. The Mabee NGL Recovery unit is a distillation columnrnwith a partial condenser and a reboiler. The condenser, operating between 4-15 oF, experienced whatrnwere described as “reflux events”, where liquid level would rapidly buildup in the reflux accumulator.rnWhile troubleshooting, it was found that hydrates formed in the top section of the column, restrictingrnthe liquid from continuing down to the next tray. The resulting buildup of liquid not only preventedrnreflux from entering the column, but also flooded the trays and quickly overwhelmed the top section ofrnthe column. This paper describes the process used to identify and address the formation of hydrates inrnthe top section of the distillation column and the use of process simulation modelling combined withrnplant data to improve plant operability.
机译:1990年代初期,雪佛龙公司在其Rangely Weber砂装置中安装了一种新工艺,用于从回收的rn CO_2中回收天然气液体(NGL)。该设备是根据1988年6月发布的专利(美国专利号4,753,666)设计的。如该专利所要求的,该方法使用回流蒸馏塔来生产实际上不含正丁烷和较重组分的塔顶料流以及包含大部分较重组分的塔底物流。基于Rangley工厂的成功运营,Dickson Process Systems设计和制造了一个类似的设施,并在得克萨斯州米德兰附近的雪佛龙Mabee油田安装了该设备。 ,布莱恩研究与工程(BR&E)和美国苏尔寿化工公司(Sulzer Chemtech USA)帮助解决该过程,以使其按设计运行。 Mabee NGL回收装置是带有部分冷凝器和再沸器的蒸馏塔。在4-15 oF之间运行的冷凝器经历了被称为“回流事件”的事件,在该事件中液位会在回流蓄能器中迅速积聚。在进行故障排除时,发现在塔顶部分形成了水合物,从而限制了继续向下到下一个纸盘。所形成的液体堆积不仅阻止回流进入色谱柱,而且使塔板充满,并迅速淹没了色谱柱的顶部。本文介绍了用于识别和解决蒸馏塔顶部的水合物形成过程,以及使用过程模拟模型和工厂数据来提高工厂可操作性的过程。

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