首页> 外文会议>Fiftieth Annual Southwestern Petroleum Short Course; Apr 16-17, 2003; Lubbock, Texas >UTILIZATION OF A CRYSTALLIZED HYDRATING COPOLYMER TO MODIFY AN INJECTIVITY PROBLEM IN A HORIZONTAL CO_2 WAG INJECTOR IN THE SOUTH COWDEN UNIT, ECTOR COUNTY, TEXAS - POST TREATMENT COIL TUBING ACIDIZING STIMULATION - CASE HISTORY
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UTILIZATION OF A CRYSTALLIZED HYDRATING COPOLYMER TO MODIFY AN INJECTIVITY PROBLEM IN A HORIZONTAL CO_2 WAG INJECTOR IN THE SOUTH COWDEN UNIT, ECTOR COUNTY, TEXAS - POST TREATMENT COIL TUBING ACIDIZING STIMULATION - CASE HISTORY

机译:德克萨斯州南部科特登州水平CO_2瓦斯注水井中结晶化加氢共聚物的利用,以修正注入问题—处理后盘管酸化模拟—案例历史

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An open-hole completed lateral CO_2 WAG injection well in the San Andres formation had not performed as desired in developing a sweep of upper structure pay and indications were that an injection profile problem existed. It was ascertained that all injection fluids were entering into a known 30-40 ft. interval approximately 230 ft from the toe of this 1,337-ft horizontal lateral rendering the remaining lateral section ineffective. Tracer surveys and interference pressure tests showed most injection fluids were being lost out of the productive interval and not giving the desired response to offset producers. A conformance design utilizing a dehydrated crystallized copolymer was implemented to control the loss of injection fluids into the unwanted zone. With confirmation of a positive treatment response, a coil tubing stimulation utilizing 135℉heated acid was performed to improve injectivity into the desired intervals within the remaining lateral section.
机译:San Andres地层的裸眼完井CO_2 WAG侧向注井在开发上部构造层时不如预期,表现出存在注入剖面问题。可以确定的是,所有注入流体都进入了一个已知的30-40英尺间隔,距离该1,337英尺水平侧面的脚趾约230英尺,从而使其余侧面无效。示踪剂调查和干扰压力测试表明,大多数注入液在生产间隔内流失了,并且对胶印生产商的响应并不理想。实施了利用脱水结晶共聚物的一致性设计,以控制注入流体进入不良区域的损失。确认治疗反应为阳性后,进行了利用135℉加热的酸进行的连续油管增产,以改善在剩余侧向剖面内所需间隔的注入能力。

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