首页> 外文会议>European Fluid Machinery Congress; 20060423-26; Hague(NL) >Upgrading of a boiler feed pump in a UK coal fired power station
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Upgrading of a boiler feed pump in a UK coal fired power station

机译:英国燃煤电站锅炉给水泵的升级

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This paper presents a case history of upgrading a series of boiler feed pumps (BFP) in a UK 2000 MW coal fired power station where life cycle costs (LCC) were used to justify capital investment. In light of the deregulation of the UK electricity industry, power stations needed to become flexible in generating load and operating times, with numerous start/stops and part-load operation becoming the norm. At Fiddlers Ferry a coal-fired power station commissioned in the 1960's, the fundamental design of a 12,000 kW (BFP) and aging associated ancillary equipment, led to significant reliability problems when faced with these new operating demands. Moreover the power station had been given a finite life and the associated reduction in maintenance spend further aggravated the situation. However with the increasing cost of gas, and relatively low price of coal, older fossil fired power stations became more economical to run. Faced with this situation Flowserve worked with the customer to understand the root causes of the pump and system problems. Flowserve proposed an upgrade solution, used LCC to calculate the reduced maintenance and operating cost on a return on investment (ROI) basis. The increased reliability/availability is expected to significantly increase the pumps' mean time between overhaul (MTBO) to 70,000 hrs (eight years). The first of the upgraded pumps is now installed, operating very satisfactorily and assisting in the generation of 25e MW more than with the original BFP.
机译:本文介绍了在英国2000 MW燃煤电站升级一系列锅炉给水泵(BFP)的案例历史,该电站使用生命周期成本(LCC)来证明资本投资的合理性。鉴于英国电力行业的放松管制,发电厂需要在发电负荷和运行时间方面变得更加灵活,大量的启动/停止和部分负荷运行已成为常态。在Fiddlers Ferry于1960年代投产的燃煤电站,其12,000 kW(BFP)的基本设计以及与之相关的老化辅助设备在面对这些新的运行要求时导致了严重的可靠性问题。此外,该电站的寿命有限,维护费用的相应减少进一步加剧了这种情况。但是,随着天然气成本的上涨和煤炭价格的相对较低,老式的化石发电站的运行变得更加经济。面对这种情况,福斯与客户合作,了解泵和系统问题的根本原因。福斯提出了一种升级解决方案,使用LCC来基于投资回报率(ROI)计算减少的维护和运营成本。可靠性/可用性的提高有望大大提高泵的平均检修时间(MTBO)至70,000小时(八年)。现在已安装了第一批升级后的泵,运转非常令人满意,与原始BFP相比,其发电量提高了25e MW。

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