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Revamp of Liaohe's Ammonia Plant with KRES Technology to reduce natural gas usage

机译:采用KRES技术改造辽河氨厂以减少天然气用量

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Shenzhen Liaohe Tongda Chemicals Co. Ltd. (Liaohe) has been operating a conventional KBR technology based 1000 MTPD ammonia plant since 1978 at Panjin City in Liaoning province China. The plant has been facing a natural gas supply curtailment leading to very low capacity utilization and reduced production. In 2001 Liaohe awarded KBR a contract to supply technology and basic engineering for a project to revamp this plant to reduce natural gas consumption from 9.15 to 6.47(expected) Gcal/MT by replacing the existing fired primary reformer with KRES (KBR Reforming Exchanger System) and maintain capacity of 1070 mtpd ammonia. An offsite coal fired package boiler was provided to maintain steam balance. Beside increased capacity utilization of ammonia plant and saving on the overall fuel bill, Liaohe also expected increased production of CO_2 by 13% and consequent higher urea production. Liaohe's KRES unit is based on a significantly improved version of the original design used for Methanex's 350 mtpd ammonia plant at Kitimat, British Columbia, Canada. Several optimized and enhanced features have been incorporated in its design. The commissioning and operating experience at Liaohe has re-confirmed all the outstanding attributes of the KRES at Kitimat All the technology enhancements, including scalability, have performed per design. The unit is very operator friendly, flexible and it adapts well to varying throughput requirements. The Liaohe revamp project has met all its expected goals. KRES offers new generation of proven technology alternative to the conventional reformer furnace. The purposes of this paper are to overview the KRES technology and provide project execution, design, commissioning and operating experience on the Liaohe's KRES unit at Panjin.
机译:深圳市辽河通达化工有限公司(辽河)自1978年以来一直在中国辽宁省盘锦市经营基于传统KBR技术的1000 MTPD氨厂。该工厂一直面临着天然气供应缩减的问题,导致产能利用率极低且产量下降。 2001年,辽河授予KBR一份合同,为该厂的改建项目提供技术和基础工程,以通过用KRES(KBR重整交换器系统)替代现有的一级燃烧重整炉,将天然气的消耗量从9.15 Gcal / MT降低到6.47(预期)。并保持1070 mtpd氨的生产能力。提供了一个场外燃煤成套锅炉,以保持蒸汽平衡。除了提高氨厂的产能利用率并节省总体燃料费用外,辽河还预期将CO_2的产量提高13%,并因此提高尿素的产量。辽河的KRES装置是基于Methanex位于加拿大不列颠哥伦比亚省Kitimat的350吨/天氨水装置的原始设计的显着改进版本。它的设计中包含了几个优化和增强的功能。辽河的调试和运营经验再次证实了Kitimat KRES的所有突出属性,所有技术增强功能(包括可伸缩性)均按设计执行。该装置非常易于操作,灵活,可以很好地适应不断变化的产量要求。辽河改建工程已达到预期目标。 KRES提供了替代传统重整炉的成熟技术的新一代替代品。本文旨在概述KRES技术,并提供盘锦辽河KRES装置的项目执行,设计,调试和操作经验。

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