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Implementing Membrane Bioreactor Technology to Upgrade Marathon Petroleum's Detroit Refinery Wastewater Treatment

机译:实施膜生物反应器技术以升级马拉松石油的底特律炼油厂废水处理

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The refining process consumes a large amount of water, mainly for cooling and steam generation systems, and produces wastewater from the various process steps. Refineries are now faced with both the challenges of discharge standards becoming more stringent and freshwater supply becoming increasingly scarce and costly. The ability to treat wastewater to higher standards to then reuse the treated effluent as process water is becoming an increasingly attractive option for refineries. Membrane Bioreactor (MBR) technology is a proven process for treating refinery wastewater to stringent requirements enabling the reuse of the effluent within the process. Marathon Petroleum Company LP (MPC) has a refinery in Detroit, Michigan, with a capacity of 132,000 barrels per day. Originally, the facility included wastewater pretreatment that was Induced Gas Flotation followed by Sand Filtration, discharging to the municipal sewage system. In 2011, a new discharge requirement was established with volatile organic compound (VOC) removal, the primary constituent being Benzene. As a result, MPC decided to move forward with a four-month pilot study using MBR technology. After successfully demonstrating consistent effluent quality below the new discharge standards, MPC proceeded with the design and installation of a full-scale, 4 million gallons per day MBR. The full-scale facility has now been in operation for over a year and has consistently achieved the performance required.
机译:精炼过程消耗大量的水,主要用于冷却和蒸汽发生系统,并从各个过程步骤中产生废水。现在,炼油厂既面临排放标准日益严格的挑战,又面临淡水供应日益短缺和昂贵的挑战。处理水达到更高标准,然后再将处理后的废水作为工艺用水再利用的能力,对于精炼厂而言正变得越来越有吸引力。膜生物反应器(MBR)技术是一种经过验证的工艺,用于处理精炼厂废水以满足严格的要求,可在工艺中对废水进行再利用。马拉松石油公司LP(MPC)在密歇根州底特律拥有一家炼油厂,日产能为132,000桶。最初,该设施包括废水预处理,先进行诱导气浮,然后进行沙滤,然后排入市政污水系统。 2011年,通过去除挥发性有机化合物(VOC)确立了新的排放要求,主要成分是苯。结果,MPC决定使用MBR技术进行为期四个月的试点研究。在成功证明废水质量低于新的排放标准后,MPC进行了每天400万加仑的全尺寸MBR的设计和安装。全面的设施现已投入使用一年以上,并始终达到所需的性能。

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