首页> 外文会议>23rd International Pump Users Symposium 2007 >VIBRATION FIELD PROBLEM RESOLVED WITH ANALYTICAL DIAGNOSTICS APPROACH AND INNOVATIVE IMPELLER DESIGN
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VIBRATION FIELD PROBLEM RESOLVED WITH ANALYTICAL DIAGNOSTICS APPROACH AND INNOVATIVE IMPELLER DESIGN

机译:解析诊断方法和创新叶轮设计解决的振动领域问题

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Several pump units of the same design installed in various locations in the USA with different duties exhibited high vibrations above API limits with process fluids (SG = 0.5 to 0.6) from rated point down to minimum continuous flow. The investigation for root cause was conducted along two parallel paths: experimental and theoretical. On the experimental side a series of shop vibration tests and modal analysis was carried out at full operational speed and cold water (SG = 1.0). These tests included: pump as installed and two modifications of the bearing housings. With the theoretical approach several computer codes of hydraulic analysis were used for analytical diagnosis in order to identify the internal hydraulic phenomena inducing the vibrations. Unsteady hydraulic forces, very likely associated with impeller discharge recirculation, were eventually considered to produce the hydraulic excitation for high vibrations. The strategy for the ultimate solution was based on a new hydraulic design impeller with innovative geometry, I.e., two blade rows with five vanes at inlet and nine vanes at outlet. Shop tests at full operational speed confirmed both the expected pump curve and presented vibrations levels (overall and vane pass) drastically reduced below API limits in the whole operating range, from rated flow down to minimum continuous flow. The new impeller was installed in all sites keeping the existing bearing housings. Field vibration data with the new impeller were collected at different times in a one year period and are compared with data produced by the old impeller. The field vibration levels with the new innovative impeller have been drastically reduced for both the overall amplitude and at vane pass frequency. The key hydraulic design parameter appears to be a high number of vanes at the impeller outlet.
机译:在美国不同地点安装的几种具有相同设计的泵单元,其不同的工作负荷,从额定点到最小连续流量,都出现超过API限值的剧烈振动,过程流体(SG = 0.5至0.6)。根本原因的调查是通过两个平行的途径进行的:实验和理论。在实验方面,在全运行速度和冷水(SG = 1.0)下进行了一系列车间振动测试和模态分析。这些测试包括:已安装的泵和对轴承箱的两次修改。通过理论方法,使用了几种液压分析计算机代码进行分析诊断,以识别引起振动的内部液压现象。最终考虑到很可能与叶轮排放再循环相关的不稳定液压会产生高振动的液压激励。最终解决方案的策略基于具有创新几何形状的新型液压设计叶轮,即两排叶片,入口处有五个叶片,出口处有九个叶片。在全速运行状态下的车间测试确认了预期的泵曲线和所呈现的振动水平(整体和叶片通过)在从额定流量到最小连续流量的整个工作范围内都大大降低到API限值以下。新的叶轮安装在所有保留现有轴承箱的位置。一年内在不同时间收集了新叶轮的现场振动数据,并将其与旧叶轮产生的数据进行了比较。对于整体振幅和叶片通过频率,新型创新叶轮的现场振动水平已大大降低。关键的液压设计参数似乎是叶轮出口处的叶片数量很多。

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