首页> 外文会议>The 17th International Conference on Fluidized Bed Combustion May 18-21, 2003 Jacksonville, Florida >REVAMPING OF 4 x 58 MWTH PULVERIZED COAL-FIRED BOILERS WITH CIRCULATING FLUIDIZED BED FIRING
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REVAMPING OF 4 x 58 MWTH PULVERIZED COAL-FIRED BOILERS WITH CIRCULATING FLUIDIZED BED FIRING

机译:带循环流化床燃烧的4 x 58 MWTH煤粉锅炉改造

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摘要

A techno-economic feasibility study has been conducted to investigate revamping four 58 MWth (15 MWe) pulverized-coal (PC) boilers with circulating fluidized bed (CFB) firing. The steam generators at Amarkantak Thermal Power Station in Chachai, Madhya Pradesh, are owned by Madhya Pradesh State Electricity Board (MPSEB), supplied by Simmering-Graz-Pauker AG of Vienna, Austria, and commissioned in mid-1965. The study reveals that: (ⅰ) CFB revamping of the boilers is technically feasible and economically sound; (ⅱ) Performance improvement of the plant is significant in terms of such indices as plant load factor, forced outage and auxiliary oil consumption, among others. The expected performance improvement is due in large part to the elimination of key outage-prone components such as pulverizers (mills) and burners, (ⅲ) There is significant improvement in emissions performance due to the reduction in emissions of NO_x and fly ash; (ⅳ) The financial analysis indicates that the CFB revamping option gives the highest return on investment compared to alternatives.
机译:已经进行了一项技术经济可行性研究,以研究改造具有循环流化床(CFB)燃烧的四台58兆瓦(15 MWe)的粉煤(PC)锅炉。中央邦查恰阿马克塔克热电厂的蒸汽发生器由中央邦电力局(MPSEB)拥有,由奥地利维也纳的Simmering-Graz-Pauker AG提供,并于1965年中期投入使用。研究表明:(ⅰ)锅炉的CFB改造在技术上可行且经济上合理; (ⅱ)在工厂负荷系数,强制停机和辅助油耗等指标方面,工厂的绩效显着提高。预期的性能改善在很大程度上是由于消除了易碎的关键组件,例如粉碎机(磨粉机)和燃烧器。(ⅲ)由于减少了NO_x和粉煤灰的排放,排放性能有了显着改善; (ⅳ)财务分析表明,与其他方案相比,CFB改造方案具有最高的投资回报率。

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