首页> 外文会议>10th International Conference on Nuclear Engineering, Vol.1, Apr 14-18, 2002, Arlington, Virginia >STEAM GENERATORS REPLACEMENT AND POWER UPRATE AT TIHANGE 2 POWER PLANT
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STEAM GENERATORS REPLACEMENT AND POWER UPRATE AT TIHANGE 2 POWER PLANT

机译:TIHANGE 2电厂的蒸汽发生器更换和功率提升

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The Belgian Tihange 2 nuclear power plant went into commercial operation in 1983 producing a thermal power of 2785 MW. In 1995, the thermal power output was increased up to 2905 MW and the fuel cycle extended to 15 months. Since the commissioning of the plant, the steam generators U-tubes have been affected by primary stress corrosion cracking. In order to avoid further degradation of the performance and an increase in repair costs, Electrabel, the owner of the plant, decided in 1997 to replace the 3 steam generators. This decision was supported by the feasibility study performed by Tractebel Energy Engineering which demonstrated that an increase of 10% of the initial power was achievable together with a fuel cycle length of 18 months. Tractebel Energy Engineering was entrusted by Electrabel to manage the project. A multi-contract strategy was adopted. The new steam generators, designed by Mitsubishi, allow raising the thermal power to 3064MW which is 110% of the initial power by an increase of the primary to secondary heat transfer area. The safety analyses necessary to justify the new operation point and the fuel cycle extension to 18 months were performed by Framatome in association with Tractebel Energy Engineering. The work on site took place during the summer of 2001 and was managed by Tractebel Energy Engineering. The SG replacement itself was performed in 17.5 days by Westinghouse PCI and the plant was reconnected to the grid on August 11, after an outage of 63 days (grid to grid). This paper presents various aspects related to the steam generators replacement project, such as the safety analysis program together with the various works on site, project management, organization, and scheduling.
机译:比利时的Tihange 2核电站于1983年投入商业运行,产生2785 MW的火力。 1995年,火力输出增加到2905兆瓦,燃料循环延长到15个月。自工厂投产以来,蒸汽发生器的U型管已受到一次应力腐蚀开裂的影响。为了避免性能进一步下降和维修成本增加,工厂所有者Electrabel在1997年决定更换3台蒸汽发生器。 Tractebel Energy Engineering进行的可行性研究支持了这一决定,该研究表明,将初始功率提高10%,并且燃料循环时间为18个月。 Tractebel能源工程公司受Electrabel委托来管理该项目。采用了多合同战略。由三菱公司设计的新型蒸汽发生器可通过增加一次到二次的传热面积,将热能提高到3064MW,这是初始功率的110%。 Framatome联合Tractebel Energy Engineering进行了证明新操作点和将燃料循环延长至18个月所需的安全分析。现场工作于2001年夏季进行,由Tractebel Energy Engineering管理。 SG更换本身是由Westinghouse PCI在17.5天内完成的,并且在停电63天(并网后)后,该工厂于8月11日重新连接到电网。本文介绍了与蒸汽发生器更换项目相关的各个方面,例如安全分析程序以及现场工作,项目管理,组织和调度等各种工作。

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