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首页> 外文期刊>Journal of natural gas science and engineering >Enhancement in NGL production and improvement in water dew point temperature by optimization of slug catchers' pressures in water dew point adjustment unit
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Enhancement in NGL production and improvement in water dew point temperature by optimization of slug catchers' pressures in water dew point adjustment unit

机译:通过优化水露点调整单元优化SLUIN捕获器压力的NGL生产和改善水露点温度的提高

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The water dew point adjustment is one of the most important processes in all gas refineries which reduces the water content of gas to some allowable limit and separates the heavy hydrocarbons from gas. In Sarkhun gas refinery, natural gas dehydration and hydrocarbon dew point adjustment are performed by cooling method. Diethylene glycol (DEC) is injected to gas-gas heat exchanger and chiller to absorb water from wet gas and act as a freezing inhibitor. Hydrate formation in filter elements was observed in this gas refinery which has been investigated in this research. The pressure difference between slug catchers and well streams were optimized by steady state process simulation software in order to decrease the mole percentage of C_(6+) exited along with the outlet gas stream from slug catcher and maximize the separation of liquid hydrocarbons. The pressure difference between the slug catcher unit and well streamlines was adjusted at optimized conditions and the experimental sampling was performed during modifications. The experimental results showed a considerable decrease in the mole percentage of C_(6+) exited along with the outlet gas stream from slug catcher and the simulation results showed 16500 bbl/year increase in NGL production rate. Operating under optimized pressure in the dew point adjustment unit of Sarkhun gas refinery decreased the water dew point temperature to -26 °C and improved the hydrocarbon dew point temperature to -9 °C. Moreover, NGL and LPG production rates increased annually about 18672 ton and 6365 ton after modifications which results in $11 million extra annual income for company.
机译:水露点调整是所有气体炼油厂中最重要的过程之一,可将气体的水含量降低到一些允许的极限,并将重质烃与气体分离。在Sarkhun气体炼油厂中,通过冷却方法进行天然气脱水和烃露点调节。将二甘醇(DED)注入气体换热器和冷却器以吸收来自湿气体的水,并用作冷冻抑制剂。在本研究中已经研究过的这种气体炼油厂中观察到过滤元素中的水合物形成。通过稳态过程模拟软件优化了块捕获器和孔流之间的压力差,以降低与来自SLUG捕手的出口气流一起退出的C_(6+)的摩尔百分比并最大化液体烃的分离。在优化条件下调节块捕获器单元和良好的流线之间的压力差,并且在修饰期间进行实验取样。实验结果表明,与SLUG捕手的出口气流一起出口的C_(6+)的摩尔百分比下降,仿真结果显示了NGL生产率的16500 bbl /倍。在Sarkhun气体炼油厂的露点调节单元中经过优化的压力,将水露点温度降至-26℃并将烃露点温度改善至-9℃。此外,NGL和LPG生产率每年增加约18672吨,修改后6365吨,这导致了1100万美元的公司年收入。

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