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Simulation of a Cold Gas Thmster System and Test Data Correlation

机译:冷气炉系统的仿真与测试数据的相关性

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During developmental testing of the Ascent Abort 1 (AA-1) cold gas thruster system, unexpected behavior was detected. Upon further review the design as it existed may not have met the requirements. To determine the best approach for modifying the design, the system was modeled with a dynamic fluid analysis tool (EASY5). The system model consisted of the nitrogen storage tank, pressure regulator, thruster valve, nozzle, and the associated interconnecting line lengths. The regulator and thruster valves were modeled using a combination of the fluid and mechanical modules available in EASY5. The simulation results were then compared against actual system test data. The simulation results exhibited behaviors similar to the test results, such as the pressure regulators response to thruster firings. Potential design solutions were investigated using the analytical model parameters, including increasing the volume downstream of the regulator and increasing the orifice area. Both were shown to improve the regulator response.
机译:在Ascent Abort 1(AA-1)冷气推进器系统的开发测试中,检测到意外行为。经过进一步审查,设计可能不符合要求。为了确定修改设计的最佳方法,使用动态流体分析工具(EASY5)对系统进行了建模。系统模型由氮气存储罐,压力调节器,推进器阀,喷嘴和相关的互连管线长度组成。调节阀和推进器阀是结合使用EASY5中可用的流体模块和机械模块来建模的。然后将仿真结果与实际系统测试数据进行比较。仿真结果显示出与测试结果类似的行为,例如压力调节器对推进器点火的响应。使用分析模型参数研究了可能的设计解决方案,包括增加调节器下游的体积和增加孔口面积。两者均显示可改善调节剂反应。

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