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Experimental investigation of a pilot-scale jet bubbling reactor for wet flue gas desulphurisation

机译:用于湿法烟气脱硫的中试喷射鼓泡反应器的实验研究

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摘要

In the present work, an experimental parameter study was conducted in a pilot-scale jet bubbling reactor for wet flue gas desulphurisation (FGD). The pilot plant is downscaled from a limestone-based, gypsum producing full-scale wet FGD plant. Important process parameters, such as slurry pH, inlet flue gas concentration of SO2, reactor temperature, and slurry concentration of Cl- have been varied. The degree of desulphurisation, residual limestone content of the gypsum, liquid phase concentrations, and solids content of the slurry were measured during the experimental series.The SO2 removal efficiency increased from 66.1% to 71.5% when the reactor slurry pH was changed from 3.5 to 5.5. Addition of Cl(in the form of CaCl2 . 2H(2)O) to the slurry (25 g Cl-/l) increased the degree of desulphurisation to above 99%, due to the onset of extensive foaming, which substantially increased the gas-liquid contact area. An increase in the inlet flue gas SO2 concentration from 502 to 991 ppmv led to a decrease in the SO2 removal efficiency from 80.1% to 69.4%. A temperature increase from 296 to 323 K caused a reduction in the degree of desulphurisation from 69.4% to 68.1%, but this result is almost within the experimental uncertainty. The residual limestone level in the gypsum formed increased with increasing values of reactor slurry pH, inlet flue gas SO2 concentration, and slurry concentration of Cl-. (C) 2003 Elsevier Ltd. All rights reserved.
机译:在目前的工作中,在用于湿法烟气脱硫(FGD)的中试喷射鼓泡反应器中进行了实验参数研究。该中试工厂从石灰石基石膏生产的全规模湿法烟气脱硫工厂进行了规模缩小。重要的工艺参数,例如浆料的pH值,SO2的进口烟气浓度,反应器温度和Cl-的浆料浓度已经改变。在实验系列中测量了脱硫程度,石膏的残余石灰石含量,液相浓度和浆液中的固体含量。当反应器浆液的pH从3.5变为3.5时,SO2去除效率从66.1%增至71.5%。 5.5。由于开始大量发泡,因此向浆液(25 g Cl- / l)中添加Cl(以CaCl2·2H(2)O的形式)使脱硫度提高至99%以上,这大大增加了气体的产生-液体接触面积。进口烟道气中SO2的浓度从502 ppmv增加到991 ppmv,导致SO2去除效率从80.1%降低到69.4%。温度从296 K升高到323 K导致脱硫度从69.4%降低到68.1%,但是该结果几乎在实验不确定性之内。石膏中残留的石灰石含量随反应器浆液pH值,进口烟气SO2浓度和Cl-浆液浓度的增加而增加。 (C)2003 Elsevier Ltd.保留所有权利。

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