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Installation caused flow distortion and its effect on noise from a fan designed for turbofan engines

机译:安装导致流量畸变及其对涡轮风扇发动机风扇的噪声的影响

摘要

A ground test stand was used to obtain acoustic data on a full scale prototype fan designed for quiet subsonic aircraft engines. The fan was installed in three different ways in the test stand. In two of the installations the fan was driven by a shaft in the inlet; in the third installation the fan was driven from the rear. These three installations, and the structures associated with them, resulted in various amounts of inlet flow distortion to the fan. The rear drive installation had less inlet flow distortion than the two front drive installations. Some measurements of inlet flow distortion were made and used in a blade passage noise generation theory to predict the effects of distortion on noise. Good agreement was obtained when the predicted and measured power level differences between the front drive and rear drive installations were compared.
机译:地面试验台用于获得为安静的亚音速飞机发动机设计的全尺寸原型风扇的声学数据。风扇以三种不同的方式安装在测试台上。在其中的两个装置中,风扇由进风口中的轴驱动。在第三个安装中,风扇是从后部驱动的。这三个装置以及与之相关的结构导致风扇的进气流量发生各种变形。与两个前驱动器装置相比,后驱动器装置的进气流量失真小。进行了一些进气流畸变的测量,并将其用于叶片通道噪声产生理论中,以预测畸变对噪声的影响。比较前驱动器和后驱动器装置之间的预测功率水平和测量功率水平差异,可以很好地达成共识。

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