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Sideslip-induced static pressure errors in flight-test measurements

机译:飞行测试测量中侧滑引起的静压误差

摘要

During lateral flight-test maneuvers of a V/STOL research aircraft, large errors in static pressure were observed. An investigation of the data showed a strong correlation of the pressure record with variations in sideslip angle. The sensors for both measurements were located on a standard air-data nose boom. An algorithm based on potential flow over a cylinder that was developed to correct the pressure record for sideslip-induced errors is described. In order to properly apply the correction algorithm, it was necessary to estimate and correct the lag error in the pressure system. The method developed for estimating pressure lag is based on the coupling of sideslip activity into the static ports and can be used as a standard flight-test procedure. The estimation procedure is discussed and the corrected static-pressure record for a typical lateral maneuver is presented. It is shown that application of the correction algorithm effectively attenuates sideslip-induced errors.
机译:在V / STOL研究型飞机的横向飞行测试演习中,观察到静压中的较大误差。对数据的研究表明,压力记录与侧滑角的变化密切相关。两种测量的传感器均位于标准的空中数据鼻梁上。描述了一种基于在圆柱体上潜在流动的算法,该算法被开发用于校正压力记录中的侧滑引起的误差。为了正确应用校正算法,有必要估算和校正压力系统中的滞后误差。用于估计压力滞后的方法基于侧滑活动与静态端口的耦合,可以用作标准的飞行测试程序。讨论了估算程序,并给出了典型横向操纵的修正静压记录。结果表明,校正算法的应用有效地减小了侧滑引起的误差。

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