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Redesign and Test of an SSME Turbopump for the Large Throat Main Combustion Chamber

机译:大型喉咙主要燃烧室的SSME涡轮泵的重新设计和测试

摘要

The preburner oxidizer turbopump for the Space Shuttle Main Engine (SSME) was successfully redesigned for use with the Large Throat Main Combustion Chamber (LTMCC) and tested in air utilizing rapid prototyping. The redesign increases the SSME's operating range with the current Main Combustion Chamber (MCC) while achieving full operational range with the LTMCC. The use of rapid prototyping and air testing to validate the redesign demonstrated the ability to design, fabricate and test designs rapidly and at a very low cost.
机译:用于航天飞机主机(SSME)的预燃器氧化剂涡轮泵已成功重新设计,可与大喉管主燃烧室(LTMCC)一起使用,并通过快速原型在空气中进行了测试。重新设计可通过当前的主燃烧室(MCC)扩大SSME的运行范围,同时通过LTMCC实现完整的运行范围。使用快速原型制作和空气测试来验证重新设计,证明了能够以非常低的成本快速设计,制造和测试设计的能力。

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