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Design, Fabrication, and Test of a LOX/LCH4 RCS Igniter at NASA

机译:NASA的LOX / LCH4 RCS点火器的设计,制造和测试

摘要

A workhorse liquid oxygen-liquid methane (LOX/LCH4) rocket igniter was recently tested at NASA Glenn Research Center s (GRC) Research Combustion Laboratory (RCL). These tests were conducted in support of the Reaction Control Engine (RCE) development task of the Propulsion and Cryogenics Advanced Development (PCAD) project. The igniter was a GRC in-house design used to evaluate the ignition processes for LOX/LCH4. The test matrix was developed to examine the flammability of LOX/LCH4 over a range of oxidizer-to-fuel mixture ratios, both in the core fuel flow and total flow. In addition, testing also examined the durability of the hardware by accumulating ignition pulses. Over the course of testing, a total of 1402 individual ignition pulses were successfully demonstrated over the range of mixture ratios. Testing was halted after the failure of the ceramic in the igniter spark plug.
机译:最近在NASA格伦研究中心(GRC)研究燃烧实验室(RCL)测试了一种主力液态氧-液态甲烷(LOX / LCH4)火箭点火器。进行这些测试是为了支持推进和低温先进开发(PCAD)项目的反应控制引擎(RCE)开发任务。点火器是内部GRC设计,用于评估LOX / LCH4的点火过程。开发了测试矩阵,以检查在核心燃料流量和总流量中,氧化剂与燃料混合比在一定范围内,LOX / LCH4的可燃性。此外,测试还通过累积点火脉冲来检查硬件的耐用性。在测试过程中,在混合比范围内成功证明了总共1402个单独的点火脉冲。点火器火花塞中的陶瓷失效后,停止测试。

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