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Gainful utilization of spent pot lining – A hazardous waste from aluminum industry

机译:有效利用废锅衬里–铝行业的有害废物

摘要

Spent Pot Lining (SPL) or Spent Cathode is a solid waste produced by the aluminium industry during the manufacture of aluminum metal in electrolytic cells. After 3-7 years ofudoperation, the cathode liner materials deteriorate and affect the cell’s performance and need to be replaced. Due to high fluoride (20 wt. %) and cyanide (1 wt. %) content SPL was listed as hazardous waste by the US Environmental Protection Agency in the year 1988.In the present study, various approaches in the treatment of SPL have been conducted to recover the valuable carbon and fluoride values. Initially a comparative study was investigated by the chemical leaching of water washed SPL with H2SO4 and HClO4 acids and the process parameters were optimized via utilization of Multiple Level Factorial design. For H2SO4 and HClO4 treatment of water washed SPL, L/S ratio was found to be the most significant factor.The carbon content was increased from 42.19% for raw SPL to 70.83% for H2SO4 and 71.76% HClO4 treatment. An approach in chemical leaching of water washed SPL was performed initially with caustic leaching followed by Perchloric acid leaching. In this case, the Temperature was found to be the most significant factor among all the parameters, whereas the L/S ratio was the least significant among the four parameters studied.The carbon percentage of SPL was increased from 42.19 to 87.03% as confirmed from the ultimate analysis. From the proximate analysis, the fixed carbon was increased from 38.96% to 82.86% from the raw to final treated SPL. Another approach in chemical leaching of water washed SPL was conducted initially with causticleaching followed by sulfuric acid leaching. In thisudcase, Alkali concentration and the Temperaturewere found to be the most significant and least significant factor among the four parameters studied.The process parameters used inudabove approaches were optimized by Taguchi method and Classical Method.The carbon percentage of SPL was increased from 42.19% to 81.27% as confirmed from the ultimate analysis. From the proximate analysis, the fixed carbon was increased from 38.96% to 78.68% for sulfuric acid from the raw to final treated SPL.Gross calorific values (GCV) wereuddetermined for the all optimized samples obtained from above studies. The GCV was found to be increased from 2865.04kcal/kg to 6689.69 kcal/kg for raw SPL and optimized sample obtained from caustic followed by sulfuric acid treatment respectively.
机译:废锅衬里(SPL)或废阴极是铝工业在电解槽中制造铝金属时产生的固体废物。经过3-7年的使用,阴极衬里材料会变质并影响电池的性能,因此需要更换。由于氟化物含量高(20 wt。%)和氰化物(1 wt。%),SPL在1988年被美国环境保护署列为危险废物。在本研究中,已采用了多种方法来处理SPL进行以回收宝贵的碳和氟值。最初,通过用H2SO4和HClO4酸对水洗过的SPL进行化学浸出研究了一项比较研究,并通过利用多级因子设计优化了工艺参数。对于水洗的SPL的H2SO4和HClO4处理,L / S比是最重要的因素。碳含量从原始SPL的42.19%增加到H2SO4和71.76%HClO4处理的70.83%。首先用苛性碱浸提,然后是高氯酸浸提,进行水洗SPL的化学浸提方法。在这种情况下,发现温度是所有参数中最重要的因素,而L / S比在所研究的四个参数中最不重要.SPL的碳百分比从42.19增加到87.03%最终分析。根据最近的分析,从原始的SPL到最终处理的SPL,固定碳从38.96%增加到82.86%。化学沥滤水洗的SPL的另一种方法是先进行碱浸,然后进行硫酸淋滤。在这种情况下,发现碱浓度和温度是所研究的四个参数中最显着和最不显着的因素。通过田口方法和经典方法对 dabove方法中使用的工艺参数进行了优化,增加了SPL的碳含量经最终分析确认,从42.19%增至81.27%。从最近的分析来看,硫酸从原始到最终处理的SPL的固定碳含量从38.96%增加到78.68%。从上述研究获得的所有优化样品的总热值(GCV)已确定。发现原始SPL的GCV从2865.04kcal / kg增加到了6689.69 kcal / kg,从苛性碱中进行硫酸处理得到的优化样品的GCV分别提高了。

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    Parhi Sidharth Sankar;

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  • 年度 2014
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