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An Experimental Investigation of a Four Inlet, Side Dump Combustor of a Kerosene - Fuelled Boosted Ramjetud

机译:煤油助燃冲压喷气发动机的四进气侧排式燃烧器的实验研究

摘要

An experimental investigation of a four-inlet side dump combustor configuration suitable for a boosted ramjet has been carried out. Combustor characteristics were obtained from water tunnel simulation and direct-connect combustion tests. A perspex, one third scale, model of the ramjet combustor was tested in a water rig. Flow field visualisation was accomplished by employing the hydrogen bubble streak technique. The best placement of the cruciform flameholder relative to the air inlet plane was determined. A similar combustor was made from stainless steel and tested in a combustor test rig. Combustion efficiency, cold and hot total pressure loss and ignition characteristics and lean blow-out limits were obtained. A design methodology for ramjet combustors has been arrived at.
机译:已经对适用于升压冲压喷气发动机的四入口侧卸料燃烧室构型进行了实验研究。燃烧器特性是通过水洞模拟和直接连接燃烧测试获得的。在水钻机中测试了有机玻璃,三分之一比例的冲压喷气发动机燃烧室模型。流场可视化是通过采用氢气泡条纹技术实现的。确定了十字形火焰保持器相对于进气平面的最佳位置。相似的燃烧室由不锈钢制成,并在燃烧室测试装置中进行了测试。获得了燃烧效率,冷热总压损失和点火特性以及稀薄吹出极限。冲压喷气式燃烧器的设计方法已经到达。

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