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Case study and back analysis of a residential building damaged by expansive soils

机译:膨胀土破坏住宅建筑的案例研究和反分析

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摘要

This paper presents a case study of a residential house damaged by expansive soils. The field investigation revealed that the damage was most likely caused by excessive lawn watering and leaks of sewer pipe and/or stormwater pipe, which resulted in non-uniform soil moisture conditions. Three-dimensional back analysis of this distressed structure indicated that stresses were most critical at a re-entrant corner and that steel reinforcing bars in the beam in this area had yielded. The results of the back analysis also indicated that a stronger footing was required to limit differential deflection to an acceptable level and reduce stress in the footing. The case study has clearly shown that a leaking underground water pipe and/or excessive watering of a garden could cause more severe distortion to a single storey masonry veneer house than could be expected from seasonal moisture change and the deeper moisture re-distribution caused by the imposition of the house on seasonally dry reactive soil. Moreover it has been demonstrated that it would be extremely costly to design a footing for extreme, or abnormal, moisture changes.
机译:本文以膨胀土破坏的住宅为例。现场调查表明,损坏很可能是由于草坪过度浇水以及下水道和/或雨水管泄漏造成的,这导致土壤湿度条件不均匀。对这种受困结构的三维反向分析表明,应力在凹角处最为关键,并且该区域梁中的钢筋已经屈服。反向分析的结果还表明,需要更牢固的基础以将微分挠度限制在可接受的水平并减少基础的应力。案例研究清楚地表明,地下水管的泄漏和/或花园的过多浇水,可能会比单季砖石单板房屋造成的严重变形严重,而季节性湿度变化和含水层重新分配会导致更深的水分分布将房屋放置在季节性干燥的活性土壤上。此外,已经证明,设计用于极端或异常湿度变化的基础的成本非常高。

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    Li J; Cameron D; Ren G;

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  • 年度 2013
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