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Process analysis and improvement of a Claus unit of an existing gas plant

机译:现有煤气厂克劳斯装置的工艺分析和改进

摘要

This research is a part of Master degree research programme at Cranfield Universityto study Claus process and perform process analysis on an existing Sulphur recoveryunit in a gas plant.The Mellitah Plant, in Western Libya, is a gas plant designed to treat raw gas andcondensate from offshore gas fields in several processing units where the sour gas(H2S, CO2, COS, SC2) is removed to meet the international emission standard, in orderto control the emission and pollution from the flue gas. The acid gases are treated inClaus unit where H2S is converted to sulphur in multi-reaction steps. These reactionsstart in a combustion reaction zone, thermal reactor, to produce a suitable mixture ofH2S to SO2. The mixture reacts in Claus catalytic reactors to produce sulphur vapour.The sulphur vapour is condensed in multi-condensing steps after each catalyticreactor.The ultimate aim of this research is to carry out the process analysis for Claus unit inorder to recover the waste energy to increase the plant productivity, minimise the useof the plant utilities, and decrease the environmental pollution. A process model of theplant was developed and validated in Aspen HYSYS. The process was then analysed,the analysis has resulted in a significant increase in Claus unit overall conversion ratiowhich has increased from 61% to 97.63% H2S base. Consequently, Claus unitproductivity has increased by approximately 1.72 times. In addition, a higher amountof energy is recovered in a form of heat by heating the boiler feed water to produceboth high pressure steam in the waste heat boiler and low pressure steam in 1st and2nd sulphur condensers. Both high pressure and low pressure steam total productionare increased by 1.5 times. All this has been achieved at high conversion ratio numberof 2 in tail gas which represents optimum O2/H2S ratio in the thermal reactor feed andthe high conversion number can be kept in between 1.5 to 3 during plant normaloperation.
机译:这项研究是克兰菲尔德大学(Cranfield University)硕士学位研究计划的一部分,旨在研究克劳斯工艺并在一家天然气厂中的现有硫回收装置上进行工艺分析。位于利比亚西部的Mellitah工厂是一家天然气厂,旨在处理来自海上的原气和冷凝水为了控制烟气的排放和污染,在几个处理单元的气田中,去除了酸性气体(H2S,CO2,COS,SC2)以满足国际排放标准。酸性气体在克劳斯装置中处理,在此装置中,硫化氢在多步反应中转化为硫。这些反应在燃烧反应区热反应器中开始,以生成合适的H2S与SO2的混合物。混合物在克劳斯催化反应器中反应产生硫蒸气。每个催化反应器之后,硫蒸气在多个冷凝步骤中冷凝。本研究的最终目的是对克劳斯装置进行工艺分析,以回收废物能量以增加排放量。提高工厂生产率,减少工厂公用设施的使用并减少环境污染。在Aspen HYSYS中开发并验证了工厂的过程模型。然后对该过程进行了分析,分析结果表明,克劳斯装置的总转化率显着提高,从H2S基准的61%提高到97.63%。因此,克劳斯单位生产率提高了约1.72倍。另外,通过加热锅炉给水以在废热锅炉中产生高压蒸汽以及在第一硫冷凝器和第二硫冷凝器中产生低压蒸汽,以热的形式回收大量能量。高压和低压蒸汽的总产量均增加了1.5倍。所有这些都是在尾气中的2的高转化率数下实现的,这代表了热反应器进料中的最佳O2 / H2S比,并且在工厂正常运行期间可以将高转化率保持在1.5到3之间。

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    Gharsalla Khaled R. M.;

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  • 年度 2016
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