首页> 美国政府科技报告 >RESULTS OF DYNAMIC STABILITY TESTS CONDUCTED ON A.012 SCALE MODEL MODIFIED 089 B SHUTTLE 0RBITER IN THE AEDC-VKF TUNNEL 3 AT A MACH NUMBER OF 8.0 (LA42)
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RESULTS OF DYNAMIC STABILITY TESTS CONDUCTED ON A.012 SCALE MODEL MODIFIED 089 B SHUTTLE 0RBITER IN THE AEDC-VKF TUNNEL 3 AT A MACH NUMBER OF 8.0 (LA42)

机译:在aEDC-VKF隧道3中修改的a.012尺度模型修改了089 B尺寸模型的动态稳定性测试结果在机械数量为8.0(La42)的情况下进行了测试

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摘要

Experimental aerodynamic investigations were conducted during June and July 1974 on a .012 scale model of a NASA/Langley modified version of the Rockwell 089B Space Shuttle Orbiter. The modification consisted of using the 139 B orbiter nose forward of station 500 on the 089 B fuselage. Using the forced oscillation test technique, dynamic stability derivatives were measured in the pitch, yaw and roll planes at a Mach number of 8 over an angle of attack range from -4° to 28°. Plotted and tabulated results are presented herein.

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  • 年度 1975
  • 页码 1-47
  • 总页数 47
  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类 工业技术;
  • 关键词

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