首页> 美国政府科技报告 >Stardust Entry Reconstruction
【24h】

Stardust Entry Reconstruction

机译:星尘入口重建

获取原文

摘要

An overview of the reconstruction analyses performed for the Stardust capsule entry is described. The results indicate that the actual entry was very close to the pre-entry predictions. The capsule landed 8.1 km north-northwest of the desired target at Utah Test and Training Range. Analyses of infrared video footage and radar range data (obtained from tracking stations) during the descent show that drogue parachute deployment was 4.8 s later than the pre-entry prediction, while main parachute deployment was 19.3 s earlier than the pre-set timer indicating that main deployment was actually triggered by the backup baroswitch. Reconstruction of a best estimated trajectory revealed that the aerodynamic drag experienced by the capsule during hypersonic flight was within 1 of pre-entry predications. Observations of the heatshield support the pre-entry estimates of small hypersonic angles of attack, since there was very little, if any, charring of the shoulder region or the aftbody. Through this investigation, an overall assertion can be made that all the data gathered from the Stardust capsule entry were consistent with flight performance close to nominal pre-entry predictions. Consequently, the design principles and methodologies utilized for the flight dynamics, aerodynamics, and aerothermodynamics analyses have been corroborated.

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号