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Large Engine Technology (LET) Task XXXVII Low-Bypass Ratio Mixed Turbofan Engine Subsonic Jet Noise Reduction Program Test Report

机译:大型发动机技术(LET)任务XXXVII低旁路比混合涡轮风扇发动机亚音速喷气噪声降低程序测试报告

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摘要

NASA Glenn Research Center supported a three year effort to develop the technology for reducing jet noise from low-bypass ratio engines. This effort concentrated on both analytical and experimental approaches using various mixer designs. Computational Fluid Dynamics (CFD) and MGB predictions are compared with Laser Doppler Velocimetry (LDV) and noise data, respectively. While former predictions matched well with data, experiment shows a need for improving the latter predictions. Data also show that mixing noise can be sensitive to engine hardware upstream of the mixing exit plane.

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