首页> 美国政府科技报告 >Moving-Bed Gasification-Combined-Cycle Control Study Volume 2:Results and Conclusions, Case 2- Oxygen-Blown, Slagging Ash Operation
【24h】

Moving-Bed Gasification-Combined-Cycle Control Study Volume 2:Results and Conclusions, Case 2- Oxygen-Blown, Slagging Ash Operation

机译:移动床气化 - 联合循环控制研究第2卷:结果和结论,案例2-氧气吹扫,结渣灰分操作

获取原文

摘要

A computer simulation study has been conducted to investigate the process dynamics and control strategies required for operation of an oxygen-blown, slagging, moving-bed gasifier combined cycle (GCC) power plant in a utility power system. The gasifier modeled is of the modified Lurgi type as developed by the British Gas Corporation. This study is a continuation of a study on moving-bed GCC control analysis. Work reported on previously (EPRI report AP-1740) was for an air-blown, dry-ash Lurgi GCC power plant and results are compared to this study.nThe simulated GCC plant configuration is similar to that developed in earlier EPRI economic studies (EPRI report AF-642). The computer model used in the air-blown, dry-ash GCC study was re-configured to represent the oxygen-blown slagging GCC cleanup process and a new gasifier model included. Gas turbine-lead and gasifier-lead control modes were evaluated with respect to power system dynamic requirements. The effect of gasifier output fluctuations, as observed in actual gasifier process development unit operation, was modeled and investigated.

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号