首页> 美国政府科技报告 >Development and Flight Test of an Active Flutter Suppression System for the F-4F with Stores. Part I. Design of the Active Flutter Suppression System.
【24h】

Development and Flight Test of an Active Flutter Suppression System for the F-4F with Stores. Part I. Design of the Active Flutter Suppression System.

机译:具有商店的F-4F主动颤振抑制系统的开发和飞行试验。第一部分主动颤振抑制系统的设计。

获取原文

摘要

Extensive research programs have been conducted at MBB and at AFWAL to investigate the application of active controls for the suppression of wing/store flutter. A flutter suppression system was developed and flight tested on an F-4F aircraft. The control law was designed by MBB using optimal control theory to minimize the control surface motion and to provide the required stability margins. During the test it was found that the dynamic behavior of the wing-pylon-store changed considerably with excitation amplitude due to free play and preload. The active flutter suppression system worked well and provided an increase in flutter speed. (Author)

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号