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首页> 外文期刊>Power Technology and Engineering >BEHAVIOR OF THE DAM OF THE SAYANO-SHUSHENSKAYA HYDROPOWER PLANT BEFORE AND AFTER RECONDITIONING
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BEHAVIOR OF THE DAM OF THE SAYANO-SHUSHENSKAYA HYDROPOWER PLANT BEFORE AND AFTER RECONDITIONING

机译:水YAN水生植物水库大坝改造前后的行为

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After filling of the storage reservoir of the Sayano-Shu-shenskaya HPP in 1989 it became obvious that the parameters characterizing the condition of the dam exceed the design values. Horizontal tensile cracks appeared on the pressure face of the dam and the contact in the foundation of the pressure face was disturbed (Fig. 1). The seepage through the dam concrete and though the foundation reached 520 and 549 liters/sec, respectively. The absence of bottom sluices did not permit emptying of the reservoir, and it was necessary to restore the water impermeability at a head of over 200 m. The high level of seepage did not allow the workers to use traditional grouts for injection. Workers of the HPP together with specialists of the Lengidroproekt Institute and representatives of the Soletange Company (France) developed a new process for reconditioning with the use of epoxy grouts. Pilot repair operations on the dam body began in 1995 and continued in 1996. After curing cracks in the body of the concrete dam, workers of the Sayano-Shushenskaya HPP continued to recondition the contact between the dam and the rock bed.
机译:在1989年填满Sayano-Shu-shenskaya HPP的蓄水池后,很明显,表征大坝状况的参数超过了设计值。大坝的压力面上出现水平拉伸裂缝,压力面基础上的接触受到干扰(图1)。穿过大坝混凝土的渗水和穿过基础的渗水分别达到520升/秒和549升/秒。没有底部水闸不允许排空水库,有必要恢复200 m以上水头的不透水性。高度的渗漏不允许工人使用传统的水泥浆进行注射。 HPP的工人与Lengidroproekt研究所的专家以及Soletange公司(法国)的代表共同开发了一种使用环氧灌浆进行修复的新工艺。大坝主体的先导维修工作始于1995年,并于1996年继续进行。在修复了混凝土大坝主体的裂缝后,Sayano-Shushenskaya HPP的工人继续修复大坝与岩床之间的接触。

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