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Girth weld integrity evaluation on a vintage gas pipeline

机译:老式燃气管道的环焊缝完整性评估

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ALEAK ON A GIRTH WELD was detected on a 609.6-mm (24-in) diameter transmission gas pipeline while recoating works were being performed. Failure analysis determined that the leak was caused by a pre-existing defect in the girth weld which had not been evolving over time. Nonetheless, because of the particular stress condition to which the gas pipeline was subject during the recoating work, the defect destabilized and progressed to failure.rnIn order to reduce the risk of occurrence of similar failures, a total of 27,000 girth welds were individually analysed, corresponding to a length of 191 kms (118 miles) of the same gas pipeline section.The analysis included evaluation of internal-inspection runs and girth-weld gammagraphs available from the recoating work. Hence, not only were the data analysed individually, but a comparison of the different sources of information to find a correlation was also performed.rnFeatures detected in the analysis were classified and prioritized base on comparison with the failed girth-weld defect. Also, correspondence with crack-like indications was considered.The severity of the anomalies was categorized on four levels.A set of the most severe crack-like anomalies with potential for failure were selected for direct assessment.rnThe complete process involved the assessment of 399 anomalies in total, revealing cracks on 79 girth welds. Metal reinforcements were installed as permanent repairs on 27 girth welds according to repair criteria, and direct-assessment findings were used to correlate internal inspection signals with features.rnThis paper discusses the results of the analysis, the field findings, and the actions taken.
机译:在进行重涂工作时,在直径609.6毫米(24英寸)的输送气体管道上检测到环焊缝上的ALEAK。失效分析确定泄漏是由环焊缝中预先存在的缺陷引起的,该缺陷没有随着时间的推移而发展。尽管如此,由于气体管道在重涂过程中受到的特殊应力条件,缺陷不稳定并发展为失效。为了降低发生类似失效的风险,单独分析了总计27,000个环缝焊缝,对应于同一天然气管道段的191公里(118英里)的长度。分析包括对内部检查运行的评估以及重涂工作可获得的环缝焊伽马图。因此,不仅要对数据进行单独分析,而且还要对不同信息源进行比较以找到相关性。在分析中检测到的特征会根据与失败的环焊缝缺陷进行比较并进行优先排序。此外,还考虑了与裂纹状迹象的对应关系,将异常的严重程度分为四个级别,选择了一组最可能发生故障的最严重裂纹状异常进行直接评估.rn整个过程涉及399次评估总共出现异常,在79个环焊缝处发现裂纹。根据修复标准,在27个环焊缝上安装了金属补强材料作为永久性修复,并使用直接评估的结果将内部检查信号与特征关联起来。本文讨论了分析结果,现场发现和采取的措施。

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