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首页> 外文期刊>Journal of bridge engineering >Forensic Examination of a Noncomposite Adjacent Precast Prestressed Concrete Box Beam Bridge
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Forensic Examination of a Noncomposite Adjacent Precast Prestressed Concrete Box Beam Bridge

机译:非复合邻近预制预应力混凝土箱梁桥的法医检验

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摘要

On the evening of December 27, 2005 the fascia beam supporting the east side parapet wall of the third span of the Lake View Drive Bridge failed under the action of dead load. To gain insight into the potential causes of the failure a series of forensic analyses were conducted on the beams decommissioned from the bridge. The study correlates external observations of surface condition with internal chloride profile, depth of carbonation, and existing corrosion. The forensic investigation indicated that strand cover was reduced due to the construction methods of the time. The chloride level in the concrete at the lower layer of strands was high enough that corrosion would be expected. Chloride attack was identified to have come from the leakage of water between beams from the bridge deck surface above. Based on the research findings recommendations are made for visual inspection, and guidelines are provided for condition rating of noncomposite prestressed concrete box beam bridges.
机译:2005年12月27日晚上,在静载作用下,支撑湖景驱动桥第三跨的东侧护墙的筋膜梁失效。为了深入了解失败的潜在原因,对从桥梁退役的梁进行了一系列的法医分析。该研究将表面状况的外部观察结果与内部氯化物分布,碳化深度和现有腐蚀联系起来。法医调查表明,由于当时的施工方法,钢绞线的覆盖层减少了。钢绞线下层混凝土中的氯化物含量足够高,以至于可能会发生腐蚀。氯化物侵蚀被确定为来自上方桥面表面的梁之间的漏水。根据研究结果,提出了目视检查的建议,并为非复合预应力混凝土箱梁桥的工况等级提供了准则。

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