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首页> 外文期刊>Environmental Technology >Efficiency of a locally designed pilot-scale trickling biofilter (TBF) system in natural environment for the treatment of domestic wastewater
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Efficiency of a locally designed pilot-scale trickling biofilter (TBF) system in natural environment for the treatment of domestic wastewater

机译:在自然环境中本地设计的中试滴滤生物滤池(TBF)系统处理生活污水的效率

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In the present study, a cost-effective and simple stone media pilot-scale trickling biofilter (TBF) was designed, constructed and operated in a continuous recirculation mode for wastewater treatment with a hydraulic flow rate of 1.2L/min (Q=0.072m(3)/h) and hydraulic loading (Q/A) of 0.147m(3)/day for 15 weeks at a temperature range of 14.5-36 degrees C. A substantial reduction in the average concentration of different pollution indicators, such as chemical oxygen demand (COD) (85.6%), biochemical oxygen demand (BOD5) (85.6%), total dissolved solid (TDS) (62.8%), total suspended solid (TSS) (99.9%), electrical conductivity (EC) (15.1%), phosphates (63.22%), sulfates (28.5%) and total nitrogen (TN) (34.4%), was observed during 15 weeks of operational period. Whereas a considerable average increase in the levels of dissolved oxygen (DO) (63.2%) was found after treatment of wastewater by the TBF system. No significant reduction in most probable number (MPN) index of fecal coliforms was observed in the effluent in first 9 weeks of operation. However, a significant reduction in the MPN of fecal coliforms was observed, i.e. 80-90% in the last few weeks of treatment. Thus, overall results suggest that pilot-scale TBF has a great potential to be transferred to field scale for treating sewage for small communities in developing countries, in order to produce effluent of good quality, which can be safely used for irrigation as well as ornamental purposes.
机译:在本研究中,设计,建造和建造了一种经济高效且简单的石头培养基中试滴滤生物滤池(TBF),该滤池以连续再循环模式进行处理,以1.2L / min的水力流量处理水(Q = 0.072m (3)/ h)和0.147m(3)/天的水力负荷(Q / A)在14.5-36摄氏度的温度范围内持续15周。不同污染指标的平均浓度(例如,化学需氧量(COD)(85.6%),生化需氧量(BOD5)(85.6%),总溶解固体(TDS)(62.8%),总悬浮固体(TSS)(99.9%),电导率(EC)(在手术期间的15周内观察到了15.1%),磷酸盐(63.22%),硫酸盐(28.5%)和总氮(TN)(34.4%)。 TBF系统处理废水后,发现溶解氧(DO)的平均水平显着增加(63.2%)。在手术开始的前9周,未观察到粪便大肠菌群的最可能数量(MPN)指数显着降低。然而,观察到粪便大肠菌群的MPN显着降低,即在治疗的最后几周中降低了80-90%。因此,总体结果表明,中试规模的TBF具有很大的潜力,可以转移到实地规模,以处理发展中国家小社区的污水,以生产高质量的废水,可以安全地用于灌溉和观赏植物。目的。

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