首页> 外文期刊>Environmental Technology >EFFECTS OF SHOCK 2,4-DICHLOROPHENOL (DCP) AND COD LOADING RATES ON THE REMOVAL OF 2,4-DCP IN A SEQUENTIAL UPFLOW ANAEROBIC SLUDGE BLANKET/AEROBIC COMPLETELY STIRRED TANK REACTOR SYSTEM
【24h】

EFFECTS OF SHOCK 2,4-DICHLOROPHENOL (DCP) AND COD LOADING RATES ON THE REMOVAL OF 2,4-DCP IN A SEQUENTIAL UPFLOW ANAEROBIC SLUDGE BLANKET/AEROBIC COMPLETELY STIRRED TANK REACTOR SYSTEM

机译:休克2,4-二氯酚(DCP)和COD加载速率对顺序通流厌氧污泥毛毯/需氧完全搅拌釜反应器系统中2,4-DCP去除的影响

获取原文
获取原文并翻译 | 示例
       

摘要

The treatability of 2,4-dwichlorophenol (DCP) was studied in an anaerobic/aerobic sequential reactor system. Laboratory scale upflow anaerobic sludge blanket (UASB) reactor/completely stirred tank reactors (CSTR) were operated at constant 2,4-DCP concentrations, and increasing chemical oxygen demand (COD) loading rates. The effect of shock organic loading rates on 2,4-DCP, COD removal efficiencies and methane gas production were investigated in the UASB reactor. When the organic loading rate was increased from 3.6 g l~(-1) d~(-1) to 30.16 g l~(-1) d~(-1), the COD and 2,4-DCP removal efficiencies decreased from 80 to 25% and from 99 to 60% in the UASB reactor. The optimum organic loading rates for maximum 2,4-DCP (E=99-100%) and COD (E=65-85%) removal efficiencies were 25-30 and 8-20 g-COD l~(-1) d~(-1), respectively. The percentage of methane of the total gas varied between 70 and 80 while the organic loadings were 18 g-COD l~(-1) d~(-1) and 20.36 g-COD H d~(-1), respectively. During 80 days of operation, 2,4-DCP concentration was found to be below 0.5 and 0.1 mg l~(-1) in aerobic reactor effluent resulting in 78 and 100% removal efficiencies. When the hydraulic retention time (HRT) was 18.72 h, the 2,4-DCP removal efficiency was 97% in the aerobic reactor. The optimum COD removal efficiency was 78.83% in anaerobic reactor effluent at an influent COD loading rate of 7.238 g-COD l~(-1) d~(-1) while 83.6% maximum COD removal efficiency was obtained in the aerobic reactor, resulting in a total COD removal efficiency of 96.83% in the whole system. The 2,4-DCP removal efficiency was 99% in the sequential anaerobic (UASB)/aerobic (CSTR) reactor system at COD loading rates varying between 11.46 and 30.16 g-COD l~(-1)d~(-1).
机译:在厌氧/好氧顺序反应器系统中研究了2,4-二氯氯酚(DCP)的可处理性。实验室规模的上流厌氧污泥层(UASB)反应器/完全搅拌釜反应器(CSTR)在恒定的2,4-DCP浓度下运行,并增加了化学需氧量(COD)的加载速率。在UASB反应器中研究了冲击有机负荷速率对2,4-DCP,COD去除效率和甲烷气体产生的影响。当有机物负载率从3.6 gl〜(-1)d〜(-1)增加到30.16 gl〜(-1)d〜(-1)时,COD和2,4-DCP的去除效率从80降低至80在UASB反应器中为25%,从99%到60%。最大的2,4-DCP(E = 99-100%)和COD(E = 65-85%)去除效率的最佳有机负载率为25-30和8-20 g-COD l〜(-1)d 〜(-1)。甲烷在总气体中的百分比在70到80之间变化,而有机负荷分别为18 g-COD l〜(-1)d〜(-1)和20.36 g-COD H d〜(-1)。在运行80天期间,发现好氧反应器流出物中的2,4-DCP浓度低于0.5和0.1 mg l(-1),导致去除效率为78%和100%。当水力停留时间(HRT)为18.72 h时,好氧反应器中2,4-DCP的去除效率为97%。在进水COD负载率为7.238 g-COD l〜(-1)d〜(-1)的条件下,厌氧反应器废水的最佳COD去除效率为78.83%,而好氧反应器的最大COD去除效率为83.6%。整个系统的总COD去除效率为96.83%。在顺序厌氧(UASB)/好氧(CSTR)反应器系统中,COD加载速率介于11.46和30.16 g-COD l〜(-1)d〜(-1)之间时,2,4-DCP去除效率为99%。

著录项

  • 来源
    《Environmental Technology》 |2008年第4期|413-421|共9页
  • 作者

    A. Ulukoey; D.T. Sponza;

  • 作者单位

    Dokuz Eyluel University, Engineering Faculty, Environmental Engineering Department, 35160, Buca Kaynaklar Campus, Tinaztepe Izmir, Turkey;

    Dokuz Eyluel University, Engineering Faculty, Environmental Engineering Department, 35160, Buca Kaynaklar Campus, Tinaztepe Izmir, Turkey;

  • 收录信息 美国《科学引文索引》(SCI);美国《生物学医学文摘》(MEDLINE);美国《化学文摘》(CA);
  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类
  • 关键词

    aerobic completely stirred tank reactor; upflow anaerobic sludge blanket reactor; sequential; 2; 4-dichlorophenol;

    机译:有氧完全搅拌釜反应器;上流式厌氧污泥床反应器;顺序2;4-二氯苯酚;
  • 入库时间 2022-08-17 13:33:47

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号