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Numerical investigation of collapse of the Minnesota I-35W bridge

机译:明尼苏达州I-35W桥倒塌的数值研究

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The I-35 Bridge over the Mississippi River in Minneapolis, Minnesota catastrophically failed during the evening rush hour on August 1, 2007, collapsing to the river and riverbanks beneath. In the years prior to the collapse, several reports cited problems with the bridge structure. This research analytically investigated the cause of the collapse using the Applied Element Method, which recently presented its capability to study the behavior of collapsing structures. The bridge was modeled using the original construction drawings, where all the structural details were taken into consideration (steel truss, gusset plates, concrete slabs, concrete piers, etc.). All the loads at the time of collapse were taken into consideration including traffic and construction loads. It was proven that AEM was capable of analyzing and investigating the cause of collapse of the I35-W bridge. The cause of collapse was found to be the failure of the gusset plates at connections L11 and U10, which well agreed with the field investigations of the collapsed bridge. The under-designed thickness of the plates, their corrosion, and the over loading due to traffic and construction loads at time of collapse were the reasons for the bridge collapse.
机译:明尼苏达州明尼阿波利斯市的密西西比河上的I-35桥在2007年8月1日晚上高峰时段发生了灾难性的崩溃,倒塌到下面的河流和河岸。在倒塌之前的几年中,一些报告提到了桥梁结构的问题。这项研究使用应用元素方法分析性地研究了倒塌的原因,最近该方法展示了其研究倒塌结构行为的能力。桥梁是使用原始施工图建模的,其中考虑了所有结构细节(钢桁架,角撑板,混凝土板,混凝土墩等)。倒塌时的所有荷载都已考虑在内,包括交通和建筑荷载。事实证明,AEM能够分析和调查I35-W桥坍塌的原因。发现倒塌的原因是连接L11和U10处的角撑板失效,这与倒塌桥梁的现场调查非常吻合。板的厚度设计不足,其腐蚀以及坍塌时由于交通和建筑荷载而造成的超载是桥梁坍塌的原因。

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