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A study of fastener pull-through failure of composite laminates. Part 2: Failure prediction

机译:复合材料层压板紧固件穿通破坏的研究。第2部分:故障预测

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The experimental study of fastener pull-through failure in composite laminates reported in Part 1 of this paper found pull though faille to be characterized by substantial internal damage similar to that observed for low-velocity impact composite panels. Damage is manifested in form of a conical distributed new tower of matrix cracking and delaminating extending through-the-thickens from the fattener head outer edge, directed away from the fastener hole. Analysis is conducted in this paper to identify the mechanisms responsible for the matrix cracking in this region. Tensile in-plane stresses are the cause of flexural failures found elsewhere in laminates of reduced bending stiffness. Fastener pull-through failure results from the tensile strength of the resin being exceeded.
机译:本文第1部分中报道的复合材料层压板中紧固件拉拔破坏的实验研究发现,拉钩具有明显的内部损坏,类似于低速冲击复合板所观察到的。损坏以圆锥形分布的新塔的形式表现出来,基塔开裂并分层,从加肥机头外缘沿整个厚度延伸,远离紧固件孔。本文进行了分析,以确定造成该区域基体开裂的机制。平面内拉伸应力是弯曲强度降低的层压板其他地方发现的弯曲破坏的原因。紧固件的穿通失败是由于树脂的拉伸强度被超过所致。

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