首页> 外文会议>SPE International Oilfield Scale Conference and Exhibition >A Novel Solution to Remove Carbonate and Sulfate Scale in Electric Submersible Pumps,Offshore Oil Wells in the Gulf of Mexico
【24h】

A Novel Solution to Remove Carbonate and Sulfate Scale in Electric Submersible Pumps,Offshore Oil Wells in the Gulf of Mexico

机译:一种新的溶液中碳酸盐和硫酸盐等级的新溶液,墨西哥湾的海上油井中的海上油井

获取原文

摘要

In the Gulf of Mexico,an important number of wells in carbonate reservoirs produce heavy oil through electric submersible pumps(ESP).The efficiency and useful life of pumps decrease due to the formation of mineral scales inside the pumps.Study of the main scale components and their origin led to look for a scale remover that is optimal for removal and that has no detrimental effect on the ESP components.Additionally, changes in the operational procedure were implemented to decrease scale formation occurrence. Inorganic scale samples were recovered from an ESP and characterized by X-ray analysis.The scale modeling software in conjunction with water analysis provided key information to predict the scale tendency and mineral composition under reservoir and operational conditions.These analyses identified the formation of two main scale minerals: calcium carbonate(CaCO3)and calcium sulfate(CaSO4).The origin of these minerals is driven by the incompatibility of formation water with water-based drilling fluids,auto-scaling due to temperature changes occurring into the ESP equipment,and the produced water flowing through the pump. Laboratory experiments were focused on finding the appropriate scale remover that could dissolve the inorganic samples that were recovered from the ESP equipment.The screening of several products allowed identifying the chelating agent with the highest activity dissolving calcium carbonate and calcium and barium sulfate scales in a single treatment. Corrosion and sensitivity tests were carried out for the metallic and nonmetallic ESP components. These results showed that the product does not have significative effect on the different parts of the ESP equipment; compatibility tests with the heavy oil and the chelant product were also satisfactory.Because of these encouraging results,a field validation test was implemented with outstanding results-the oil well production increased significantly and the temperature in the ESP equipment was improved. The implementation of this chelating agent in wells presenting scale formation significantly improved the oil production and increased the ESP run life cycle under profitable economic indicators.The operator has implemented an operational procedure for wells operating with ESP that consists in continuous monitoring to optimize the treatments.
机译:在墨西哥湾,碳酸盐储层中的一个重要井通过电潜水泵(ESP)产生重油。由于泵内部的矿泉鳞片,泵的效率和使用寿命减少。主尺度组件的研究他们的原点导致寻找最佳删除的刻度卸液,对ESP组件没有有害影响。加法,实施过程过程的变化以减少规模形成发生。从ESP中回收无机刻度样本,并通过X射线分析表征。尺度建模软件与水分析结合提供关键信息,以预测储层和操作条件下的规模趋势和矿物质组成。该分析确定了两种主要的形成尺度矿物质:碳酸钙(CaCO 3)和硫酸钙(CasO4)。这些矿物质的起源是由形成水与水性钻井液的不相容性驱动的,由于温度变化发生在ESP设备中,自动缩放,以及生产流过泵的水。实验室实验旨在找到可以溶解从ESP设备中回收的无机样品的适当刻度去除剂。筛选几种产品,允许溶解碳酸钙的最高活性和钙和硫酸钡鳞片中的螯合剂治疗。对金属和非金属ESP组分进行腐蚀和敏感性测试。这些结果表明,该产品对ESP设备的不同部件没有有意义的影响;具有重油和螯合产品的兼容性测试也令人满意。因为这些令人鼓舞的结果,通过出色的结果实施了现场验证测试 - 油井产量显着增加,ESP设备的温度得到改善。在井中展示规模形成的康复剂的实施显着提高了石油生产,并在有利可图的经济指标下增加了ESP运行生命周期。经营者实施了井中的运营程序,其中包括持续监测,以优化治疗。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号