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Well Design and Successful Field Installation of Openhole Sand Control Completions with Acid Stimulation in a Highly Deviated Well in Vietnam

机译:在越南高度偏差良好良好良好的酸刺激下,透露孔砂完成的良好设计和成功的现场安装

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Application of openhole sand control technology is becoming mandatory in the field, particularly with the given uncertainty in geomechanics, challenges to wellbore integrity while drilling, and sand production during the life of the well. The completion equipment readiness and success of the installation can be challenging in the event of extending the horizontal section to accommodate geological heterogeneity and maximizing well productivity. This paper discusses operational excellence recorded in Well A, in the Thang Long Field, offshore Vietnam, from well design perspectives ensuring maximum reservoir contact to outcome of well completion. The well was targeted in the Oligocene reservoir, a thin oil rim with large gas cap overlay, and required drilling and completion for 1126 m horizontal length of 8 1/2-in. open hole. The completion design included multiple swellable packers for isolation of unwanted zones, 6 5/8-in. basepipe sand screens for the production zones, and a fluid loss control device to help prevent undesirable losses. Several torque and drag simulations were performed to help predict potential threats that could be encountered during completion string deployment or during space out of the inner wash pipe string. One apparent challenge of this completion design was to deploy the lower completion string to total depth (TD) per stringent reservoir requirements, resulting in an approximate 1126 m length of the string in the horizontal section. Another task was to facilitate manipulating 1130 m of wash pipe inside the completion string to locate the seal assemblies accurately at the corresponding seal bore extension positions for effective acidizing treatment. Although these were long sections of completion string and wash pipe, the quality of acidizing stimulation to effectively remove mud cake should not be compromised to ensure positive production rates. During operations, the completion string was run to target depth without any issue, and the wash pipe was spaced out and manipulated correctly. These operations subsequently led to a successful acidizing treatment and the proper closure of the flapper type fluid loss device. The completion design and operation were concluded successfully, significantly contributing to field production performance to date. The novelty of the completion design and installation is the ability to deploy an 1126-m lower completion in long, highly deviated and horizontal openhole section coupled with acid stimulation in reasonable time and as per plan.
机译:透露孔砂技术在现场成为强制性的应用,特别是在地质力学中给予的不确定性,钻井良好诚信的挑战,以及在井的生命期间的沙子生产。在延长水平部分以适应地质异质性并最大化良好的生产率时,安装的完工设备准备和成功可能具有挑战性。本文讨论了卓越的卓越,在越南近海越南,从良好的设计视角,确保最大水库与完井结果的结果。该井是针对寡替纳储层的薄型,一个薄的油轮,具有大的气体盖覆盖,并完成钻孔和完成1126米的水平长度为8/2英寸。开孔。完成设计包括多个可稳定的封隔器,用于隔离不需要的区域,6 5/8英寸。 BasePipe Sand屏幕为生产区,以及流体损耗控制装置,有助于防止不期望的损失。进行了几种扭矩和拖曳模拟,以帮助预测在完成串部署期间或在内部洗涤管柱的空间期间可以遇到的潜在威胁。这项完成设计的一个明显挑战是将较低的完成字符串部署到每个严格的库要求的总深度(TD),导致水平部分中的串的大约1126米长。另一种任务是便于操纵完成绳子内部的1130米的洗涤管,以在相应的密封孔延伸位置定位密封组件,以便有效酸化处理。虽然这些是完工串和洗手的长部分,但酸化刺激的质量不应妥协,以确保正生产率。在操作期间,完成字符串运行到​​目标深度而没有任何问题,并且洗涤管子被隔开并正确操纵。这些操作随后导致成功的酸化处理和挡板式流体损失装置的适当闭合。完成设计和运营成功结束,迄今为止达到现场生产性能。完成设计和安装的新颖性是能够在长度,高度偏差和水平的露出部分中展开1126-M次完成,并在合理的时间和计划中加上酸刺激。

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