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Thermal efficiency improvement and technology transfer of chimney stove for producing stove; Amphoe Bo Kluea, Nan Province

机译:烟囱炉生产炉灶的热效率提升及技术转让; Amphoe Bo Kluea,南省

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Salt production by evaporation of brine drawn from deep wells in of Bo Kluea District, Nan, has been carried out for many centuries by using traditional wood-based stoves. This study aims to improve thermal efficiency of traditional stoves, while tradition stove structures and salt making methods were maintained. The prototype and tradition stove were compared by thermal efficiency method. The tradition stove was constructed with clay. The prototype chimney stoves have been making from brick plastered with cement. The prototype chimney stove was insulated by filling rich hush in the gap of stove wall which has 3 cm. thicknesses and the end of the chimney. The stove can put 2 pans. Eucalyptus woods were used be fuel for testing the thermal efficiency. The prototype stove increases thermal efficiency approximately by 5.3 percents form normally 9.6 percents. This is achieved by using carbonized rice husk as stove insulating materials to reduce heat loss through stove walls. Salt production cycles are decreased by 25 minutes from 4.5-5 hours and the rate of fuel per day decreased 14-15 kilograms from 257 kg of firewood. Costs to improve salt production stoves 1,545 THB have a Pay-back period 107 days. The improved prototype chimney stove can help to decrease fuel costs and increase the salt production rate. This research is not only saving energy but also keep tradition of local living.
机译:通过蒸发来自南·南·南·克利亚区的深井,通过使用传统的木制炉子进行了多个世纪的盐水生产。本研究旨在提高传统炉灶的热效率,而传统炉子结构和盐制造方法得到了维持。通过热效率方法进行比较原型和传统炉。传统炉子用粘土构建。原型烟囱炉炉一直从砖块涂抹水泥。通过填充炉墙间隙的富裕呼吸,原型烟囱炉在具有3厘米的炉子的间隙中被绝缘。厚度和烟囱的末端。炉子可以放2平方平底锅。使用桉树木材是燃料,用于测试热效率。原型炉子大约提高了5.3种百分比的热效率通常为9.6%。这是通过使用碳化的稻壳作为炉子绝缘材料来实现的,以减少通过炉墙的热量损失。盐生产循环从4.5-5小时减少25分钟,每天燃料率降低14-15千克木柴。改善盐生产炉的成本1,545个THB有157天的薪水期。改进的原型烟囱炉可以帮助降低燃料成本并提高盐生产率。这项研究不仅节省了能源,还保留了当地生活的传统。

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