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A REFINERY APPROACH TO ADDRESS CORROSION UNDER INSULATION EXTERNAL CORROSION

机译:绝缘和外部腐蚀下地址腐蚀的炼油厂方法

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Corrosion under Insulation (CUI) and External Corrosion continue to be a major issue for all Petrochemical facilities throughout the world. Over many years, refineries and petrochemical plants have experienced extensive damage due to these mechanisms. As a result, several of the company refineries have been investing in a CUI and External Corrosion inspection program. This paper details the methodology used by two refineries for addressing this damage and lessons learned throughout the implementation.The methodologies used by the two refineries differed at first in that one approach involved an initial cursory inspection of all areas in the refinery and history review of all fixed equipment items followed by a thorough inspection and maintenance refurbishment of equipment selected by this initial inspection. The second approach involved a software based desk top study with no initial inspection. The programs are being managed as a total refurbishment project, which include the identification of lines and vessels operating below 350 degrees F; inspection of vessels and lines, including insulated and painted lines; 100% removal of insulation in areas ranked High and Medium High based on the assessment above; repair where necessary; repaint and finally re-insulate if necessary.The paper also describes the findings from the work carried out so far. At Refinery A whichfollowed the initial cursory inspection approach, 18 vessels have had 100% insulation removal, 200 miles of piping have been visually inspected and 16 miles of piping refurbished. For vessels, 89 areas had lost part or all of the corrosion allowance, 26 areas had undergone weld repairs, 2 tower top heads have been replaced and a further nozzle replaced. On piping, 137 areas were found to have gone through part or all of the corrosion allowance and 61 further pipe sections required replacement. At Refinery B, the areas for inspection were selected using a desk top study. The selection did not include an initial inspection of the entire refinery. The desk top study directed the efforts to discrete areas of the refinery where external conditions of insulation and long range NDE's were then used to decide whether further insulation removal was necessary. The approach at Refinery B has resulted in fewer inspection finds and it is now adjusting the CUI/External Corrosion program based on these finds and the lessons from Refinery A.
机译:绝缘腐蚀(CUI)和外部腐蚀仍然是全世界所有石化设施的主要问题。多年来,由于这些机制,炼油厂和石化厂遭受了广泛的破坏。结果,该公司的几家炼油厂一直在投资进行CUI和外部腐蚀检查程序。本文详细介绍了两个炼油厂用于解决这种损害的方法,并在整个实施过程中吸取了教训。 两家精炼厂使用的方法首先有所不同,其中一种方法涉及对精炼厂的所有区域进行初步的粗略检查,并对所有固定设备项目进行历史回顾,然后进行彻底检查和维修翻新的设备。第二种方法涉及没有初始检查的基于软件的台式研究。这些计划作为一个整体翻新项目进行管理,其中包括识别在华氏350度以下运行的管线和船只;检查船只和管路,包括绝缘和涂漆的管路;根据上述评估,在排名为“高”和“中”的区域中100%去除绝缘材料;必要时进行维修;重新粉刷并在必要时重新绝缘。 该文件还描述了迄今为止进行的工作的发现。在炼油厂A 按照最初的粗略检查方法,对18艘船的绝缘材料进行了100%去除,目视检查了200英里的管道,并翻新了16英里的管道。对于船舶,有89个区域失去了部分或全部腐蚀余量,有26个区域进行了焊接维修,更换了2个塔顶盖,并更换了另一个喷嘴。在管道上,发现137个区域已经腐蚀掉了部分或全部腐蚀余量,还有61个管道需要更换。在炼油厂B中,使用台式研究来选择检查区域。选择不包括整个炼油厂的初步检查。台式研究将工作重点放在了精炼厂的离散区域,在这些区域中,使用绝缘的外部条件和长距离NDE来决定是否需要进一步去除绝缘。炼油厂B的方法导致更少的检查结果,现在它正在根据这些发现和炼油厂A的经验教训来调整CUI /外部腐蚀程序。

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