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Rebuilding of the 70 years old Nore 1 Power Plant

机译:重建拥有70年历史的Nore 1发电厂

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At Nore 1 Power Plant the water was conducted from a low pressure head race tunnel to the above ground power house by 8 exposed penstocks of 1000 m length. For safety reasons, Norwegian authorities have ordered all so-called water gas welded penstocks to be taken out of service within certain time limits. A number of alternative schemes for the necessary rebuilding of Nore 1 were developed. The selected scheme was to replace the penstocks between the existing head race tunnel and the power house by a new underground waterway system in rock. Required rock overburden of water bearing tunnels and length of steel lined tunnel were determined by means of rock stress measurements as well as numerical analyses. Most of the tunnels were excavated by drill & blast while the power plant was in operation with the old penstocks. In the vicinity of the power house vibrations induced by blasting had to be kept within certain precalculated limits. To connect the low pressure head race tunnel to a new high pressure tunnel it was decided to excavate a vertical unlined pressure shaft of 213m length. However, the main challenge to the project was to limit outage time for the turbine units during the construction and erection period for the new system.
机译:在Nore 1电厂,水是通过8个长度为1000 m的裸露压力管从低压顶头竞赛隧道引到地面发电站的。出于安全原因,挪威当局已下令所有所谓的水煤气焊接压力管道必须在一定时限内停用。已经开发出许多必要的Nore 1重建方案。选择的方案是用岩石中的新地下水道系统代替现有的顶盖竞赛隧道和动力室之间的压力管道。通过岩石应力测量和数值分析,确定了承水隧道所需的岩层和钢衬隧道的长度。电厂使用旧压力管道运行时,大多数隧道都是通过钻爆开挖的。在动力室附近,爆破引起的振动必须保持在某些预先计算的范围内。为了将低压缸盖滚道隧道连接到新的高压隧道,决定开挖一条长度为213m的垂直无衬砌压力井。但是,该项目的主要挑战是在新系统的建造和安装期间限制涡轮机的停机时间。

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