...
首页> 外文期刊>Tunnelling and underground space technology >Shield tunnel uplift and deformation characterisation: A case study from Zhengzhou metro
【24h】

Shield tunnel uplift and deformation characterisation: A case study from Zhengzhou metro

机译:盾构隧道抬升与变形特征分析-以郑州地铁为例

获取原文
获取原文并翻译 | 示例
           

摘要

Excavation in close proximity to the existing shield tunnel often leads to impacts on the stability of tunnel. However, interventions committed to mitigate the impacts may not be effective in preventing tunnel movement and/or deformation from occurring. This study presents a case history where two shield tunnels pass between two excavation pits belonging to the east square of the existing Zhengzhou East High Speed Rail (HSR) station. The centre down-top pit retained using a series of bored piles and three rows of tieback is first excavated in each excavation pit, followed by the periphery top-down pit retained by the diaphragm wall. The tunnels measured cumulative uplift and lateral deformation being equal to 22.9 mm and 77.9 mm, respectively, as the two excavations reached the final depth of 19.3 m. The tunnels also observed ballast separation, lining crack, and joint leakage. The contribution from each of the construction stages to the tunnel uplift and deformation is analysed. The effectiveness of the rectifications adopted is assessed and the lessons learnt are summarised preventing future similar incident from reoccurring.
机译:在现有的盾构隧道附近开挖往往会影响隧道的稳定性。但是,旨在减轻影响的干预措施可能无法有效地防止隧道运动和/或变形的发生。本研究提供了一个案例历史,其中两个盾构隧道在属于现有郑州东部高铁(HSR)站东广场的两个开挖坑之间通过。首先在每个开挖坑中开挖使用一系列钻孔桩和三排系带固定的中央下顶坑,然后通过隔板墙将其周围的上下顶坑开挖。当两个开挖达到最终深度19.3 m时,隧道测得的累积隆起和横向变形分别等于22.9 mm和77.9 mm。隧道还观察到压载物分离,衬砌裂缝和接头泄漏。分析了每个施工阶段对隧道抬升和变形的贡献。评估所采取的纠正措施的有效性,并总结总结的经验教训,以防止将来再次发生类似事件。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号